|

“Preserving South Africa’s
Steam heritage for all to enjoy.’
One thing that’s remarkable about our Steam Locomotive Depot is that it is
never really all that uncomfortable to work there in terms of temperatures.
Whether it is blazing hot outside, or a grey, drizzly day, the depot
workshops and sheds remain comfortable. The only downside is trying to
remember which work benches are under rust holes in the roof and strategically
avoiding them! We had a drizzly day outside, which made things a little
slippery underfoot and made the steam action photography look a little dull
as steam doesn’t show up well against a murky grey sky. None the less, our
wonderful steam locomotives look good no matter what the weather.
We had a good turnout of Reefsteamers this Saturday and yet
it was a strangely quiet day. We worked in singles and pairs spread out all over
the sheds and there was a separate crew not involved in repairs at all, but
firing up the Class 15F No.2914 ‘Spikkels’ for a trip to Magaliesburg the
following day.
Project - Garrett Bissel Truck Bolster Slides :
The project that naturally drew the most attention during
the day was actually a unique step in South African Railway Preservation
History. This is the first time, to our knowledge, that a Vesconite Plate
has been fitted to a Steam Locomotive’s Bissel Truck.
The two bearing plates were prepared in the morning, being
marked, drilled and countersunk. And of course, the pristine white Vesconite
got very grubby in the process – so they’ll soon blend in neatly with the
black grit that crusts the underside of any locomotive! You can see the
mucky fingerprints in Pic G01. Shaun had to painstakingly match the
counter-sinking to the angle of the bolt heads. (Pic G01) Not only was this
necessary to ensure a sustained tight fit, but also to maximize the
effectiveness of the bolt’s key. These countersunk bolts have no slots or
hexes to allow for holding while tightening them up.
|

|

|

|
|
G01 – A countersunk bolt being
inserted into the Vesconite bolster slide plate to test the countersink angles.
Notice the keyway visible on the top surface of the bolt.
|
G02 – A view of a loosely assembled
Vesconite Bolster Bearing Slide. Note that the 8 countersunk bolts all
have plain, smooth featureless heads.
|
G03 – Wooden shim blocks and an
expansion jack used to press the countersunk bolts home and to engage their
keys to facilitate tightening.
|
The 19mm thick Vesconite Plates were installed into the
stripped and primered Bissel truck frame. (Pic G02) The bolts were
tightened in diagonal sequence to centralize the slide bearing to the frame
rebates. 8 Countersunk bolts were used on either side and fastened with nice,
modern nylock nuts. Even though the holes matched quite well, there was
still too much flex in the bearing plate to get the bolts to pull in and
tighten up by hand or by socket.
So, the ‘Bissel Team’ had the Catch-22 annoyance of not
being able to tighten up the bolts because the head keys didn’t ‘bite’ – and
having to tighten the stupid bolts to get the keys to bite in the first
place. The problem was resolved by bridging the central frame aperture with a
collection of wooden blocks and using a portable expansion jack to press the
bolt heads home, engage the keys and allow for proper tightening. (Pic G03)
The bolt tightening was a bit of a fiddly job and one had to watch out for
nipped fingers.
But, with fingers un-nipped, and bolts safely ‘nipped,’ eventually
the moment arrived to test the newly serviced bolster slide plate. This
required a bit of hoisting, as to suspend the plate centrally within the
Bissel’s frame. The workshop gantry crane was hooked up to the air
compressor lines. Initially, the gantry was used to clear the track so that
Class 15F No.2914 ‘Spikkels’ would be able to trundle out the shed to prepare
for the next day’s trip to Magaliesburg. Think of it as a railway version of
tidying up the slippers from the bedroom floor. We’d left a whole litter of
Bissell frames and axles spread out across the rail heads. (Pic G05) We
moved two axles and a frame, as well as dead bearings and a few scotch
blocks. (Pic G06) A surprise for us all was the amount of moisture that had
gotten into the air compressor lines – blowing out in a staccato, violent
spray. The line was gingerly held and allowed to blow clear for a while
before the clawed air line fitting was hooked up.
(Pic G04)
|

|

|

|
|
G04 – Our air compressor plant clearly
doesn’t like running on rainy days. An astonished looking Shaun lets loose
with an impressive jet of condensate blown off from a compressed air line,
before hooking up the gantry crane’s air-motor.
|
G05 – Some tidying up required.
Bits-of-Bissell lie across the track in front of Class 15F No.2914 which
was in steam and ready to leave the workshop shed. In this shot, the
original Bissel truck frame is being hoisted off its blocks.
|
G06 – With the Bissel Truck neatly out
the way, we rolled the original axle forward for lifting. Here Tony King
checks the grip of the hoist hooks around the thickset spokes as the crane
takes up the tension. That’s the Sandstone Garratt visible to the right.
|
The freshly cleaned and primered Bolster Plate was easily
managed by the pneumatic hoist, with the hooks cleanly going through the
Bolster Spring Bosses and dollied across to the waiting frame. With the
weight still taken up by the pneumatic hoist, we carefully lowered the
Bolster Plate in between the two Vesconite slides.
In a sense, it looked quite good – a freshly painted oxide-red Bolster Plate
sealing the gaping, open cavity of the Bissell frame like a neatly fitting
box lid.
The Bolster Plate lowered easily … rather too easily. Much,
much too easily.
And when things are too easy with locomotives, you get suspicious.
Uh Oh!
We found that we had the opposite problem from which we
started. Regular readers will remember that the original problem with the
GMAM Garratt’s ‘Lindie Lou’ Bissell Truck was a seized Bolster Plate caused
by the swelling effect of rust behind the original steel sliding plates,
pushing them inwards and ‘pinching’ the Bolster Plate. Now we had a plate
that was a few mils too loose. I was impressed with the guys as they hardly
even swore. They just stood around the Bissell Truck and stoically watched
the Class 15F 2914 leaving the workshop, with Andrew King giving a slow,
cynical ‘royal wave’.
The solution to the loose Bolster Plate problem was to shim
one of the plates inwards with washers.
This time, with the Bolster Plate suspended in place, measurements were made
and then a Reefsteamers scavenger hunt for washers took place. We needed
wide washers to spread the bearing load. Fender washers are too thin, and
the standard wide washers that we have collected over the years, are too
thick.
So, Dawie Viljoen was put to the tricky task of firing up the lathe and
turning several washers down to the correct thickness to act as custom made shims.
(Pic G08)
|

|

|

|
|
G07 – The sliding Bolster Plate suspended
within the waiting Bissel Frame and being checked for clearances.
|
G08 – Some tricky turning work. A
standard washer is being machined down to the correct thickness to shim up
the clearances of the new slide bearings.
|
G09 – Catch that washer! Shaun is
fishing around behind that bearing plate for an errant shim-washer while
Kenny looks on in amusement.
|
In the mean time, while master machinist Dawie was making
skinny washers and steel slivers, Lee and Kenny started the process of
loosening one of those new slide bearings again, as to be able to slip the
washers between the back face and the frame. It was amusing to see that
Kenny instinctively chose the leading plate behind the A-frame, as he had a
comfortable place to sit on the pivot eye while cracking off those bolts. This
task meant we had to set up the wood blocks and jack contraption again. The
nuts came off okay but it took a judiciously applied ball peen hammer to get
those bolts out again. The washers were inserted and lined up with the bolt
holes with a combination of finger and wire – but not without the washers
dropping right through behind the bearing plate, clunking dismally against
the Bissel Truck frame like a rejected coin passing through a vending
machine.
Well, so now the sliding Bolster Plate fits the Bissel.
The swing links, retainers and the axle guides need to be installed. And the
Bissel Frame needs to be drilled and tapped to accept some new grease nipples
to service those new bearings. There is to be a delay with the Bissel
truck’s assembly though as we need to source new axle bearings to replace the
pitted ones that we found. But, it’s great to have made some progress
towards converting the GMAM Garratt from a 4-8-0 + 2-8-4 to a 4-8-2 +
2-8-4.
Project – GMAM Garratt Stoker Motor Overhaul :
When Reefsteamers brought the Sandstone Estates Class MMMM
* Garratt back from the Rovos Rail facility, the locomotive was found to be
in decent overall running condition. We were already aware of the bad wheel
flange wear problem – which lead to the Bissel Truck removal and overhaul as
described above and in previous weeks. Another obvious fault was the fact
that the mechanical stoker was knocking like a mad carpenter. Michael Thiel
started dismantling and checking out the Stoker last week and basically found
that nearly every bearing was worn. These bearings can be rebuilt, and new
gudgeon pins fabricated, but that takes time.
* MMMM = Mr. Mole’s Magnificent Machine
|

|

|

|
|
S01 – The two-throw Stoker Crankshaft
with the donor big ends and rods being tested for fit. That is an unusual
work bench that Michael was using – with a firmly padded green vinyl top.
|
S02 – A railway Fitter doing his
‘Fitting’.
Michael’s whole attention is on the
big end bearing cap in his hands. He found it necessary to remove a small
amount of white metal from the crush points of the bearing shell liner,
which he did with a flat needle file.
|
S03 – A view of the Stoker Crankcase
awaiting its components and new Crankshaft main bearings. (Ball bearings) The
rod ends visible in the center are the for the valve eccentrics. Notice
three brass coloured areas in the casting where brazing repairs have been
made in the past.
|
Michael carefully dismantled a second, unused Standard
Stoker that we’ve had lying in the top shed for a while. The donor stoker’s
components proved be in better condition and the big end caps are in decent
shape.
So an exercise in mixing and matching components took place, with a little
traditional white metal scraping taking place. (Pic S02) The donor’s
crankshaft and main bearings were not removed. We need to source new main
bearings for the GMAM Garratt stoker – which are roller bearings, not shell
bearings as used in a car or truck engine. The removed parts will be
re-fabricated and rebuilt and then laid aside with the donor stoker to make a
complete spare unit.
Project – Class 25NC Seller’s Valve Grinding :
Steam Locomotives and leaks go together and it’s little
wonder that they are affectionately (or otherwise) called ‘tea-kettles’ by
their fans and detractors. Our locomotives are no different and we’re
constantly chasing down and trying to seal leaky valves. Leaking steam and
dribbling injector water may be picturesque but conflicts with our policy of
locomotive maintenance, as well as being wasteful of water and the energy
used to heats it. But in mitigation, one needs to remember that many of the
valves are 50-60 plus years old and high pressure steam itself has the power
to cut notches and grooves in already-leaky valve seats and fittings.
Pat Ackerman has had many years experience repairing,
restoring and driving steam locomotives on the Sandstone Estates 2ft narrow gauge
network and his expertise came in useful in fixing a stubborn injector
dribble on our Class 25NC No.3472 ‘Elize’. The engine has a double deck
arrangement for the injector water valves with stubby levers in a confined
space. These have been unpleasant to operate, trying to force them home to
reduce injector dribble. And if one uses two hands to shut that injector
off, one runs the risk of burning your right arm against the grate shaker
pipes … ask me how I know!
|

|

|

|
|
V01 – Patrick Ackerman concentrating
at his work on the Class 25NC Sellers valve. While the 25NC has a generous
overhang, the walkways aren’t that wide – he’s standing comfortably on a
scaffolding arrangement.
|
V02 – Valve Elements. You can see the
removable valve seat at the bottom, the valve desk itself and the pilot
valve being held on top. The main source of the leak was actually UNDER
the valve seat and not on the upper sealing surfaces.
|
V03 – A top quarter view of the valve
assembly with the valve disk and pilot valves removed.
|
Patrick did the conventional clean and grind operation,
using a beveled grinding cutter. However, he also found where the main leak
was – between the removable valve seat and the valve body. (Pic V02) A tiny
leak had become notched over time. Because it was under the valve seat,
grinding down the valve seat surface and the valve disk wouldn’t help one
bit. He ground down the valve body slightly, cleaned the seat and then
handed it over to the Chief Engineer, Andrew King, for inspection.
Andrew King deemed the seat unsuitable – so a spare seat
was rustled up from stores. Poor Pat had to do grinding and fitting once
more to put the bastardized valve back together, only to find that it would
still have leaked. He discovered that the diameter of the valve seat was
wider than the cutter head – thus leaving a higher un-cut ridge around the
edges and messing up the seal. The valve seat had to be turned in the lathe
to cut away the circumferential ‘crown’ ridge. The valve is now together –
but the proof of the work will be nice dry injector overflows the next time
the boiler is pressurized.
Project – Class 15F Reverser Valve Chamber
Service :
Our Class 15F No.2914 ran for the first time in a year and
4 months a few weeks ago. She did great, but as we expected, there were
issues found. (She IS a steam locomotive after all. :o) ) One issue was
damaged dynamo armature bearings due to incorrect oil being used. Another
issue was the fact that the power reverser kept creeping forward. The valve
chambers on both the actuating and the lock cylinders had been removed,
checked and serviced. It was time to put it all back together in time to get
the locomotive running this very afternoon. We frequently see Reefsteamers
fitting parts and components onto a live boiler with steam issuing from open
pipes and ports. It wasn’t long before the loco-lighting crew busy in the
cab got a peeved request from the mechanics to turn off the reverser’s turret
valve!
|

|

|

|
|
R01 – Andrew King is tapping out a new
Reverser Valve Chamber Gasket by tapping a sheet of gasket material against
the work piece with a ball peen hammer.
Those black ‘barbells’ on the bench in
front of Andrew are a valve spindle for the Class 12AR No. 1535 ‘Susan.’
We are waiting for 7 new boiler tubes before boiler prep work can
continue. The pistons need to be removed to check the rings too.
|
R02 – A freshly made brand new Reverser
Valve Chamber Gasket. Notice that one hole still needed to be pressed out
with a finger tip.
|
R03 – A newly serviced lock cylinder
valve for the Class 15F. The valve body is inverted and you can clearly
see the two rectangular slots where the oil is channelled from one end of
the cylinder to the other to allow the Reverser’s Actuator Rod to move.
Should the valve be closed (lever vertical) the trapped oil within the lock
cylinder forms a hydraulic lock on the Reverser’s actuator rod – which
keeps the locomotive in the selected valve cut-off.
|
There’s no such thing as going to Midas to get replacement
gaskets for locomotives. We roll our own! Andrew tapped out the new gaskets
by applying a sheet of gasket material to the mating surfaces and tapping gently
around all the edges and the holes with a ball-peen hammer, to indent and
thin out the gasket sheet stock along the edges. (Pic R01) It’s a classic
technique for making customized gaskets. The gentle hammer taps cut out the
edges and the peen-ball neatly cuts the holes. The gasket is then pressed
out of the sheet along the thinned and cut sections. It results in a
slightly rough cut but accurately fitting custom made gasket. And one
doesn’t need to do tedious cutting along pencil marks either! (Pic R02)
|

|

|

|
|
R04 – A brass ‘Wagon Top’ Reverser Actuator
Cylinder cover in the ‘corner vice’ have the end slots elongated to fit.
|
R05 – Reverser Actuator Cylinder with
a brass cover fitted. Note the valve itself is still in place in amongst
those studs. That pipe was steaming while the boiler was warming up but
the turret valve had already been shut off by the time this pic was taken
|
R06 – Stuart uses a conical grindstone
to elongate the end holes of the brass cover for the lock cylinder.
|
Stuart was put to the task of fitting the brass ‘Wagon Top’
cover sheets to the Class 15F Actuator and Lock Cylinders for the Power
Reverser. These units had been recently painted in the traditional signal red
for the reverser actuator and it’s rods, and traditional green for the lock
cylinder and the indicator rods. Reefsteamers prefers to use a conservative
colour scheme, your basic Persian-midnight ‘plain black’ and red buffer beams
being the safest for photography. Not every photographer likes detail or
movable parts picked out in colour. While both the valves were off and the
linkages removed the opportunity was taken to smarten the reverser up with
some brass sheeting. Stuart had to some trimming and grind stone work to get
the sheets to fit properly.
Andrew and Stuart met their tight time schedule and the Power
Reversing Gear was buttoned up and
ready to go by the time the locomotive was required to be moved for turning
and coaling.
Project – Other Locomotive Work :
The characteristic SAR ejector valve covers on the Class
15F No.2914 were removed and serviced by Kenny. These covers can be prone to
leakage and are easily damaged by over-tightening. These covers rarely leak
enough to affect the operation of the brakes themselves, but the escaping
steam constantly blows across the engine driver’s field of vision and can
burn whoever operates the brakes. Kenny managed to remove, clean and seal
the covers with only one extra trip to the store room to get a longer cheat
bar and socket. The two covers didn’t require extensive filing, grinding or
panel beating – just a little cleaning and a generous helping of ‘Stag’ pipe
sealer.
|

|

|

|
|
W01 – Kenny gets to grips with
removing ejector valve covers on the 15F No.2914. Just above Kenny’s thumb
is the Locomotive Brake and the long ‘slot machine’ lever visible to the
right is the main Train Brake.
|
W02 – Class 15F Brake Ejector assembly
with the valve covers removed. Piet Steenkamp has plans to paint that
startling blue boiler ring cover back to basic black.
|
W03 – A newly cleaned blow down valve
as patiently cleaned up by Tony King. Apart from assorted oil cups, these
are usually the lowest mounted brass components on a loco – they get
dulled, scaled and sooted rather quickly.
|
Project – Club House :
Work continued on clearing up the articulated coach set for
conversion into a club house. Lex and Willie were hard at work and a bit
isolated away from the rest of the gang. They have fitted a new Yale lock on
the coaches to keep the baddies and the doggies out. The intact compartments
are to be used for storage while the clubhouse section is being rebuilt. So
we’re preventing pilferage as well as vandalism.
|

|

|

|
|
H01 – A new brass Yale lock shines
incorigously against weathered wood. That weathered wood shows the biggest
challenge with these coaches – to prevent further decay of the wooden
structure in open storage.
|
H02 – A cleaned picture frame with
intact glass and a new set of pictures. That cleaned panelling looks good
in the picture and it hasn’t even been re-varnished yet! That patch on the
ceiling is where the coal burning stove’s chimney used to be.
|
H03 – View of the Club House Coach
interior – the scraping and the pain is beginning. You can see an intact
picture frame to the left and a folded table on the floor right at the
back.
|
An original folding table has been removed and serviced,
and is being prepared for installation, and we’re looking for some seats. In
the meantime, roof apertures have been sealed and plated off. The guys also
carefully removed one of several long, delicate ladder-like picture frames
(Pic H02) and did some cleaning and simple, smartening work by installing
new colour photographs to replace the faded, moisture damaged photos. The
old photos are to be put into safe keeping however.
Marketing :
The Marketing Gang and some board members got together to
discuss issues. Lee’s proposal for an on-board Reefsteamers Information pack
was reviewed. This is a small document to be handed out one for each family on
the train to explain a little about Reefsteamers and who we are, and where
our locomotives come from. The content was basically approved but Lee has
the challenge of cutting down his somewhat verbose writing to 5 pages
maximum. Hmmmm.
|

|

|

|
|
T01 – Marketing meeting. We were
discussing the proposed Information Pack to be handed out on the trains, as
well as articles for magazines and general strategies for advertising.
From left to right, Les Smith, Fred Sewell, Hardie Visagie, Shaun Ackerman,
Andrew King (Front) and also starring, Lee’s briefcase.
|
T02 – Keeping it simple. Day-trip coaches
are identified with a single digit printed on A4 paper. It’s a lot easier
to remember than the standard 5 digits. These can be removed for the
photographer’s trips.
|
T03 – Loading up ‘Kango’. We had the
luxury of coach keys being available, so the first lot of tuck-shop foods
and drinks could be loaded through the corridor hatch. This hatch is
conveniently located at floor level and opens straight through to the
Catering Car’s Corridor.
|
The Marketing guys also discussed the existing Reefsteamers
Trips and Sponsors Brochure, as well as managing adverts to be placed into
magazines. We are looking seriously into advertising in ‘Go’ \ ‘Weg’
magazines. Trip schedules were confirmed for the next few months as well as continuing
communication with SANRASM, using Les Smith as the point-of-contact.
In preparation for the Magaliesburg Trip on the next day,
Les Smith put up coach number signs in all the Coach doors. We have found
that day-tripper people don’t remember the standard SAR 5 digit coach
number. We have also found that people get confused when the locomotive is
turned at the end of a run, and placed on the other end of the coaches,
especially when we have a water tanker on each end of the train. They try to
sit in the same position relative to the locomotive and end up in wrong
coaches – a PR problem for the SANRASM trips where compartments are booked.
We do have an existing set of magnetic signs but some have been hooked off
the train by passing thorn tress and some have been hooked off the train by
souvenir hunters. So we’ve gone for a cheap and easily replaceable method.
And they can be removed for a more authentic look during photo tours and
trips.
Cool drinks and crisps were loaded into ‘Kango’, the
catering car, in preparation for the trip the next day. The perishables were
loaded the following morning. It’s not cost efficient to run the generator
overnight to refrigerate a few trays of eggs and a few packs of bacon.
Pictures from around the Shed :
|

|

|

|
|
M01 – Is this a wood burning
locomotive? This is a view of the firebox of Class 15F No.2914 ‘Spikkels’
with the wood fire burning merrily after being lit by the firelighters.
Marshmallows anyone?
|
M02 – The large, sprawling area of our
depot makes carrying tool boxes around to be a schlep. Mike Thiel has
combined functionality, fashion and tool security with this really neat compartmented
tool barrow.
|
M03 – White wheel rims look great but
need cleaning after every run. Shorty gets intimately acquainted with the
4-8-2 ‘Mountain’ wheel arrangement of a Class 15F.
|
|

|

|

|
|
M04 – A good motivation for roadworthy
inspections, a washout plug weeps slightly in the RHS foundation ring of
Class 15F No.2914. Gotta go get the tube socket now….
|
M05 – Class 15F No.2914 ‘Spikkels’ had
a leaky non-return valve and riser pipe union. Andrew King gets a grip on
the riser union with a ‘slogging’ spanner and a fence post that Lee Gates
found – to make a crude but very effective long-handled spanner.
|
M06 – The Last Biscuit.
A very rare sight in our Depot, a biscuit that survives more than 5
minutes! Everyone’s pride prevented them from digging in and this biscuit
survived several hours.
( Ultimately, I put the poor thing
out of it’s lonely misery. :o) )
|
|

|

|
|
|
M07 – Getting them hooked! A pair of
youngsters enjoyed a busy day of fire-lighting work, dispensing oil,
cleaning copper work, eating with ‘the train people’ and riding the engine
while it was being turned and serviced. They were still smiling in the
evening, with dirty faces fresh from the coal loading dock.
|
M08 – Driver Piet Steenkamp expected a
quiet and routine session of turning and coaling his engine. He ended up
with 5 extra passengers in his cab! (Seven people in all.)
|
|
- Lee Gates -
|