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REEFSTEAMERS INDEX PAGE
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Steam in Action – An Association Incorporated under
Section 21 – Registration Number 2007/035119/08
www.steam-in-action.com -
Email : joannewest@btinternet.com
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Reefsteamers Depot News Report
- SATURDAY, 23 February 2008 -
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Introduction :
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We had a good, productive weekend at the
depot, managing to get another one of our steam locomotives off the sick-list
and back into operation. The high focus job of the day was the re-assembly
and replacement of the overhauled front bogie for the Class 15CA No.2056
‘Dorothy’. The bogie job took a little longer than expected, but apart from
the surprise requirement to fabricate some new spacers to go between the
compensating spring casting and the bogie frame, the job went quite
smoothly. Quite a few little running maintenance jobs were done on the
locomotive on Sunday, as well as the installation of the missing cow catcher,
the lamp standards and the front steps. As I type this paragraph (out of
sequence with the rest of the doc), I’ll be heading out to the depot in about
40 minutes to take on the Friday night shift of locomotive minding. This
engine is running tomorrow and Sunday (1 and 2nd March) and we are
hoping that she will do well.
In the meanwhile, Dave Shepherd’s Class
15F No.3052 ‘Avril’ got some attention too, to start knocking off some of the
repairs from the list that was written up after her debut revenue earning for
Reefsteamers. The badly leaking power reverser’s lock cylinder was removed,
inspected and fitted with brand new seals and a correctly refaced bushing.
The coaches got their share of attention
too – a set of brake shoes being replaced and the re-wiring project spreading
to another coach. The bar car got some cosmetic work and a disused
refrigerator cavity in the management car’s kitchen is being re-fitted with
shelves.
We had an excellent turn out of volunteers
for this Depot Day, and your favourite photographer was run off his feet
trying to keep up with the groups scattered all over the Depot, all of them
volunteers and all of them working for the love of steam.
Well done guys … and thank you.
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PROJECT : Reassembling and Refitting the front bogie of
Class 15CA No.2056
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The bogie reassembly and re-fitting job
was the glamour job of the day and drew a wide audience, to the extent of
being quite difficult for your photographer to get clear, unobstructed shots.
But you can’t get too frustrated with those who have an equivalent interest
in steam engines. But many a time I had a set-up photo ruined by an arm
moving into the picture, or somebody’s white helmeted head popping into the
view finder. And clear night time shots with slow shutter speeds are rare
opportunities. Still, here is a sequence of photographs and a write up about
how we got the bogie back together. Normally, when one writes articles, or
perhaps a column in a news paper, the difficulties and the hard times make
the better stories. This was a long job with many sub tasks, but it actually
went quite smoothly.
The compensating spring casting has
already been reassembled by Andrew King and Michael Thiel the previous week,
when Michael had just come on duty to do locomotive minding – this thus becoming
an evening project. It gave the bogie team a head start on getting it all
back together again, and Michael Thiel got the time to take some care in
putting the compensating spring assembly back together again … a welcome
change from stoker engine work. The ‘temper’, leaf count and height of the
springs were all verified against a purchased set of scanned SAR drawings. Every
moving point, bearing surface and pivot was well greased and the threads were
all cleaned up and re-cut upon assembly.
The day’s Magaliesburg train came back
later that evening. Class 25(NC) No.3472 ‘Elize’ came shuffling in after
disgracing herself on the run by breaking a fire grate – a very rare
Reefsteamers breakdown. After the usual locomotive servicing was done, we
had a few more people to help put the bogie’s bolster back together. But
getting the wheels and springs back in would be left for the following week,
which is the topic of this article.
The long job started with the
straightening of the Wheel Stretchers (Compensating Beams) as the RHS set
were slightly splayed. (Pic B01 below) The stretchers were carried over to
the 50 ton press by four people, carefully laid out in the press and blocked
up at both ends. (Pic B02 below) It wouldn’t do to have this lot flipping
and twanging under pressure. Pressing the wheel stretchers straight was easy
enough once a dolly block was found. Because the ends, made of flimsy 26mm
thick steel, are unsupported, it would be only too easy to press them too far
inwards. The correctly sized dolly block was found and the ends of the frame
were pressed parallel again. However, under the pressing, the frame ends
bowed in slightly, so with the press extended and clamping the wheel
stretchers tight, the hydraulic jack was inserted in the very ends and
extended to bring them straight once more.
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B01 – You can just see the splayed ends between Shaun’s
hands, as he explains the coming job sequence to the bogie team.
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B02 – Putting the wheel stretcher in the press. You
can see the ram in front of the dark shirted operator. Notice the dolly
block placed as a spacer between the frames.
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B03 – Spreading the now-bowed ends
with the hydraulic jack, with the
main press ran extended.
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Oddly enough, only the stretcher on one side
was splayed. It looks as if the engine was driven into an excessively tight
curve at one point in her working life. It took four Reefsteamers doing a
dog-trot to get the stretcher back to the bogie frames, (Pic B04 below) which
was waiting four tracks down in the eight track workshop, and finally, the
assembly could begin. Assembly started by arranging a set of crude slides
for the compensating spring casting. While the bits were being put together,
Phillip Maurer got busy grinding down some detected high spots in the bearing
arches on the bogie frame itself. (Pic B05 below) As the bogie has been completely
dismantled, the original wear patterns will probably not line up with the
reassembled components (Even though we marked which ends and which side
everything came from) so it’s good practice to get everything smoothed down
again. The slides comprised of four assorted ‘gwala’ bars ramping up to the
rail heads and spanning the inspection pit. The entire compensating spring casting
was placed on wooden blocks and resting over the end of the gwala bar ramp –
damage to the gleaming new primer-coat paintwork was minimal. (Pic B06
below) The assembly was eased up the bars by three people, while two others
held the ends of the bars in place.
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B04 – The stretcher team hurries the patient back to
the bogie. They’re moving quickly, hence the blurred background, in order
to get there before their curled fingers give up!
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B05 – Phillip grinds off remaining high points on the
underside of the bearing arches.
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B06 – Gwala bars are useful as crude
ramps and slide rails to move heavy equipment and components around.
This big lump of ironmongery is to
move upwards and to the right.
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With the compensating spring casting precariously
in place across the pit under the bogie frame, it was time to sling up and
hoist up, before something slipped up! (Or would that be … slipped down?) A
wrinkle in this job was that the bolster, with the four massive dangling
swing links, was already in place above where the compensating spring casting
needs to go. Thus, the sling had to be passed around the entire bolster and down
past the sides. (Pic B07 below) It puts a bit more stress on the sling and
means more corners exposed to chafing. The cylindrical barrel bearing under
the bolster also had to be brought into engagement between the horizontal
leaf springs – slightly compressing them. But the job was achieved and it
wasn’t long before the four bolts that hold the casting in place were being
screwed in. Naturally, it’s a two man job with one working from underneath
and one working through the bogie frame. (Pic B08 below)
The wheel stretchers were installed next,
with the use of the rolling gantry crane. They aren’t actually physically
attached to the bogie frame – but simply rest in slots. They are always free
to move up and down and very slightly, side to side. (Pic B09 below) They
were slung into place by using the top pins. The ends needed guiding and that
was probably the most dangerous part of the job – having to watch fingers for
nipping.
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B07 – The compensating spring casting is just being
hoisted from the gwala bars spanning the pit. The hoist sling had to be
awkwardly passed around the bolster.
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B08 – A view from underneath with my head under where
the axle will eventually go - Dawie and Oom Attie are bolting up the
Compensating Spring Casting.
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B09 – The loose ends of the wheel stretchers inserted
into their slots.
Without the springs in place, these
are dropped in from above.
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While the wheel stretchers (compensating
beams) were going back in, Dawie was tasked to find some scrap tubing and cut
out two new spacer tubes. You can see a deeply inset bolt hole in the center
of Pic B08. Dawie cut two sections from a scrap super-heater element and machined
the ends. The springs and the shackle bolts were next. (Pic B11 below) Each
heavy spring had to be slid under the bogie frames sideways and then rotated
up in between the plates of the stretcher frame. Gaining clearance was easy
as the stretchers were still free to be hoisted, but the final positioning of
the springs required judicious use of the hydraulic jack to get their ends
into the shackles. The ends of the springs, as well as their upper points
were all generously lubricated with graphite grease upon re-assembly. (Pic B12
below)
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B10 - A view of an inserted new spacer through an upper
access hole in the frame. You can see where the access hole Is in relation
to the bogie frame in Pic B09.
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B11 – The leaf spring shuffle. Dawie and Phillip
shuffle a leaf spring along the floor.
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B12 – Here’s an end view of a bogie spring inserted
into an assembled shackle.
Notice the application of graphite grease!
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Meanwhile, fireman Sakkie ‘Sakana’ Kekana got
the surprise job of repainting one of the main leaf springs that we had
salvaged from the abandoned 15CA out back of the depot. (Pic B13 below) The
springs had been checked and selected by Andrew King as the closest match for
our own. Luckily, the oxide red primer is quick drying and without fumes
either. While the paint brush was being wielded, the scattered parts of the spring
retard straps were brought back together, the four bolts all had threads re-cut
and cleaned and the retard straps put back on. These retard straps serve to
retain the leaf spring safely within the frame should a spring or a shackle
break or become disengaged. (Otherwise they’d drop straight into the track
work and cause a derailment.) The job was complicated by the need to leave
the now-heavy left spring and wheel stretcher assembly from the compensating
spring casting to fit the straps behind the wheel stretchers. The bolts are
also inserted from the inside out (Pic B14 below) which means the bogie frames
have to be jacked apart from the wheel stretchers to allow the bolts to be
passed in from the interior. It’s a safety feature as it means the bolts
cannot fall out even if the nut on the outside works loose.
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B13 – Sakkie Kekana tackles a surprise painting job.
This is the salvaged leaf spring.
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B14 – A spring retard strap that has just been
refitted. Notice that the bolts fit awkwardly from the inside out as a
safety feature.
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B15 – Test fitting an oil tray. Notice that the tray
is the right way round but Dawie is putting it in through the thrust face
whereas when in situ, they normally enter from the rear. (It’s not a
mistake - He’s checking that the recessed sides of the bearing are truly
parallel without turning the machined thrust face over against the rough concrete
floor.)
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Then the work shifted to a new and more
exciting phase, the fitting of the bogie’s axles! Before this could be done,
the bearings had to be prepared and fitted. These big chunks of white metal
were brought out of stores and then matched up to each original corner from
whence they came. The oil trays (‘keeps’) were also matched up to their
relevant bearing. Even though the marks matched up, each tray was fitted to
its bearing to ensure that they still fitted. (Pic B15 above) The white
metal from which these components are made can be prone to distortion and
burring which might obstruct smooth operation. Remember that the oil trays
are usually installed or removed from under the locomotive during a service,
and with the packing, or socks, restricting the movement as well. One wants
the movement to be as free as possible. The two bearings for the front axle
were anointed, by hand, with fresh MH oil. (Pic B16 below.)
There is a bit of errata required here, as
pointed out by Shaun. In a previous Depot Report I stated that lubrication
oil flows down from the thrust face into the bearing arch. It actually moves
up and out from the bearing arch to the thrust faces that bear against the
back of the wheels. The oil is pumped up those oil galleries by the
hydrodynamic pressure of the oil between the axle and the bearing arch – thus,
the oil in the tray also constantly lubricates the thrust faces. The upwards
flowing hydrodynamic action is exactly the same, in principle, to that of a
‘rifle bored’ con-rod in an internal combustion engine, where oil is
automatically pumped from the big end to the gudgeon pin.
Okay, errata over and back to the show. With
the bearings well oiled, and the corresponding surfaces on the axles well
seasoned, they were loosely placed on the axles. Meanwhile a pair of freshly
made packing bags, what we call ‘socks’, were inserted into each cleaned tray
and drizzled with a generous, yummy coating of MH oil, even through the socks
were already impregnated with oil. In fact, on the following day, the trays
were withdrawn once more and even more oil poured in.
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B16 – An axle bearing’s thrust face is
lovingly anointed with fresh MH oil.
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B17 – Yummy! A delicious MH oil flavoured sauce is drizzled
onto a fresh pair of axle packing ‘socks’ which are full of
oil;-impregnated woollen yarn.
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B18 – An unobstructed view of a tray (or ‘keep’) being
inserted into a bearing. The fresh socks put up quite a resistance!
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The oil trays, or ‘keeps’ as we call them,
were put in their slots in the bearings. In normal circumstances, this can
be tricky as you’re duck walking and grunting under the locomotive. There
was still much grunting involved even though the axles are loose and there
weren’t even frames to obstruct movements. (Pic B18 above) The new socks
are tightly packed and put up a bit of a fight. Incidentally, this
illustrates a weak point in this type of design for a bogie bearing. When repacking
these bearings in service, any dirt on the axle ends would be wiped off by
the oil socks and introduced into the very bearing surfaces that you’re
trying to lubricate.
The top of the axle bearings incorporates
an oil chamber that is normally hidden under a thin pressed steel cover. The
chamber uses six trimmings (‘or wicks’) as per the oil pots on the motion. 4
of the wicks provide oil to the axle horn bearings. Piet Steenkamp is the ‘trim
master’ of Reefsteamers. He had fabricated and pre-soaked the trimmings in
paraffin to ‘prime’ the capillary action of the fibres. (Pic B19 below) Just
like the oil pots on the motion and valve gear, these wicks are immersed in
MH oil. The semi circular bearing pads for the tips of the wheel stretchers
were inserted as well (Pic B20 below) and then the all important oil was
added. (Pic B21 below).
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B19 – The oil reservoir with a single
fresh wick that has been inserted for a
horn guide bearing. The oval ended slot
in the foreground is a wheel stretcher
bearing pad cavity.
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B20 – All the wicks are in the empty oil chamber and
the semi-circular wheel stretcher bearing pads have been inserted, both
richly smothered in graphite grease.
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B21 – More oil please. The oil reservoir is being
filled. From this point on, the freely rotating bearing had to kept
vertical to
avoid spilling the new oil.
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The next step is to put the back covers
on, with the studs being carefully wire locked – it’s not done to have parts
just dropping off under the engine. (Pic B23 below) With the bearing
assembly and oiling work all done, it was now time to use the rolling hoist
to left up the bogie frame end and to roll the axle in between the horns.
There was some debate about the weight capacity of the hoist – but as Andrew
had safely dismantled this lot using the same equipment, all by himself over
Christmas weekend, we got on with it. (Pic B24 below) Rolling the axle on
the rails isn’t at all difficult, but the bearings have to be kept upright
when they try to revolve as well.
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B22 – A clear view of an assembled bearing with the back
covers not yet installed.
Notice the compression of the oil sock.
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B23 – The end plate studs are wire-locked.
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B24 – With the frames hoisted, the
front axle is rolled into place.
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We lowered the hoist very gently and fed
the bearing slides into the waiting (and freshly lubricated) axle horn
guides. The oil chamber covers were quickly slipped in under the descending
wheel stretcher ends. (Pic B25 below) That was one axle done and all the
work had to be done on the rear axle and its two bearings. The second axle’s
work was enlivened by the fact that it was stored out on road 7 in the depot
and still had to be rolled along the trolley tracks, manually grunted 90
degrees and then trundled along the length of the depot and then turned 90
degrees again to line up with ‘our’ bogie. It now has got some fresh
scratches on the flanges! The rolling gantry came in useful to hoist the
trailing axle and pass it over the bogie assembly. (Pic B26 below) There
wasn’t enough travel available in the hoist to clear the axle completely, and
it had to be held labourously off to one side to allow the two sets of wheels
into interleave past each other. But once the axle was safely down on the
rails again, it was time to start the bearing assembly procedure all over
again.
But there was a simultaneously annoying
and amusing hiccup in the job. The team had forgotten to put the retaining
bolts in for the cotters for the lower set of links on the swing links. And
these are very hard to get at on an assembled bogie. (Pic B27 below) There
wasn’t enough room to apply a spanner or a socket to the nut end. We all had
no choice but to stand around and watch the alternative cursing and laugher
going on – but hey, at least it was remembered.
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B25 – Steady as she goes, mind
your fingers and don’t forget the
oil chamber cover! The frame is
sliding home over the axle bearing,
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B26 – Heaving the second axle over the assembled
bogie. That’s the highest the hoist could go and the wheels had to be held
offset to clear the finished front axle.
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B27 – A hand is all you can see of Dawie as he tries to
fit a bolt through the cotter pins. The lack of clearance between the bolt
and the big chrome tie shaft made it hard to use a spanner and impossible
to use a socket.
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Well, with the bogie finished, Class 15CA
No.2056 ‘Dorothy’ still had to be prepared to accept this mechanical work of
art. The kingpin and the lubrication pipes were inspected. You can see the
general layout in Pic B28 below. There are four oil pipes that are filled
from a common oil-box on the front snuffler plate. Each pipe discharges
above the location of the four swing link pins. The center pipe discharges
into the hollow pivot pin and eventually discharges into the pivot boss. The
pipes were straightened up, blown through with compressed air and rodded
through with heavy duty baling wire. The four swing link oil pipes were
actually functioning as evidenced by the nice oily swing links discovered
upon removal, but it’s always good to take the opportunity to get the ‘kidney
stones’ out of the plumbing when one has free access like this.
The center oil pipe was a problem. It
discharges into an open top bore which had filled up with grit and sludge.
The bore discharges by gravity through a sprout and drips directly into the
swivel disks. Of course, this bore was just about totally blocked. Shaun
and Dawie spent about 30 minutes cleaning out the gunk from the chamber,
working through the very limited space you can see above the square base
plate in Pic B28. The copper pipe should have been pushed further in, and
then the hollow chamber filled with clean woolen waste around and above the
copper pipe – to act as a barrier against further dirt
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B28 – A view of the locomotive’s bogie
pivot and the lubrication lines
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B29 – A close up of the non-functional bolster-pin oil
discharge sprout. The
hollow pin casting was choked with dirt.
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B30 – One of two swivel disks
being cleaned and lubricated.
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While the dirt picking was going on,
Sakkie cleaned and lightly oiled the bolster bearing disks. (Pic B30 above)
Jacking up the locomotive was the next
task – a bit nerve wracking to watch and in which to participate. I hid
behind the camera tripod for protection. Actually, the jacking operation was
performed safely and worked well. We started from the position shown in Pic
31 below. The locomotive was jacked up with pneumatic jacks under the buffer
beam, with a collection of the ubiquitous wooden blocks shoved and shoved in
the expanding gap. The jacks were put through two full cycles, being
withdrawn halfway, their rams retracted and starting their cycle again
mounted on their own wooden blocks. Great care was taken to jack up both
sides evenly. The final height had the lowest edge of the buffer beam 1.2
meters from the ground – as assessed by me making a nervous measurement. (Pic B32 below)
Before the bogie was reinstalled,
advantage was taken of the ‘loose tooth’ wheel-less gap between the cylinders
to get some Reefsteamers under there and tighten up some bolts on the draft
gear and the buffer spring casings – some of which were found to be loose.
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B31 – The slumbering locomotive
about to get jacked beyond recognition.
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B32 – ‘Romeo Sugar – One-Five-Charlie-Alpha requests
permission to take off !’
A locomotive with attitude, or is that altitude? Us Reefsteamers really
can
make a steam loco sit up and beg!
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B33 – Wheelin’ in the bogie. Notice
that Willie ‘Sarge’ Wehmeyer has just
joined the team and gotten into the action.
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The bogie was wheeled in (Pic B33 above)
and the front gap packed up again with wooden blocks in case a jack slipped.
The engine was then carefully lowered to engage the bolster pin into its
socket. Andrew King was at home in that small space putting in the locking
pin, which was held in place with wires (Pic B34 below), which Shaun Ackerman
was holding under tension. (Pic B35 below) It looked like he was using
dental floss on the Iron Giant. Andrew had to get under that decreasing gap
and give the suspended bolster a nudge on its swing links to get everything
to line up. In spite of Shaun’s hands getting some deep groves and Andrew
bumping his nut a few times on the lowering frames, the installation went
well. The bogie boys were quite quick to break up at about 8:30pm although 6
of the die-hards decided to go out for a celebratory supper.
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B34 – The Bolster Pin is approaching the boss with the
locking pin clearly visible. Notice the two tension wires leading
off to the left. They lead out to…
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B35 –… to Shaun’s hands as he frantically tries to
retain the tension, with the wire cutting into his gloveless hands. Notice
that Shaun is sitting safely clear of the cylinders.
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B36 – The finished result – a great old engine taking
on coal on the following Friday. The smoke box braces, lamp stanctions and
cow catcher were installed the following day (Sunday) and ‘The Spoories’
applied the loco-makeup, including the gleaming white brake pipe.
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This engine was worked on some more on the
following day and here is a list of what was done :
1). The bogie horn keeps were fitted.
2). The axle box keeps were removed again and re-filled with
oil,
just to be sure of good lubrication, as the woolen oil socks soak up the
oil.
3). The ejector cone caps where removed, faced in the lathe and
re-fitted for a better seal.
4). The Bissell and Tender axle box covers were removed to check
the oil,
all the socks were turned and the boxes refilled with fresh MH oil.
5). All the fusible plugs were removed from the firebox,
re-melted and
cleaned and then re-cast before inspection, recording and re-fitment.
6). All the oil trimmings have been replaced.
7). The cow catcher was reinstalled.
8). The lamp stanchions were remounted.
9). The smoke box front braces were replaced.
10). The front steps were refitted.
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PROJECT : Conducting a boiler test on Class 15F No.3016 ‘Gerda’
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Today’s boiler related work was the third
installment in a three week saga. Actually, the boiler wasn’t tested on
Saturday, but rather, on Sunday. Saturday’s work was the removing of a
leaking siphon tube plug located in a classically awkward location. It is a
plug on the firebox front wrapper plate (Sometimes called, The ‘Throat Plate’),
right in the middle and hidden between the cylindrical boiler barrel and the
frames. It is where the belly button would be if a locomotive boiler had
one. Removing these plugs isn’t difficult on a regularly run and serviced
locomotive (aka, frequent boiler washouts), just so long as one has room to
use a Tommy bar of some kind for extra leverage. This plug, usually the
rustiest plug on a steam locomotive, had little no ‘swing room’ for a Tommy bar
of any kind. You can see the position of this somewhat rusty ‘belly button’
in Pic W01 below. You can see that there isn’t much room to work between the
locomotive frames and the objects in the front and the rear are the main
springs and the spring hangers or the rear driver axle.
A locomotive boiler, firebox and the back
plate is usually fitted with tapered plugs with square heads, on about 2 – 2
½ inches along one flat. The threads are of heavy gauge but can wear out
over the average 50-80 year lifespan that we expect as normal in the 21st
century. These plugs, scattered all over the locomotive, are removed for
boiler inspections, and more frequently, for boiler washout. Some of the
holes are used as rather sludgy drain holes and others are used to allow the
ingress of water hoses and hot water or steam lances. The siphon tube plugs
are used to de-scale and inspect the siphon tubes that span the firebox under
the fire arch. The plug heads come in various sizes, so a part of the
challenge is finding the right 80 year old tube spanner to fit the right 80
year old washout plug. The tube spanners usually only have 2 bores drilled
at 90 degrees in their drive barrels, (Pic W02 below) so, if you can’t latch
onto your square-head and turn it at least 90 degrees in the arc of one
swing, you can’t latch on for a further swing. We have some curved pinch
bars and crow bars for this purpose. (By contrast, a classic motor
mechanic’s crescent spanner has a head that can be offset by merely 15
degrees if you flip the head over.)
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W01 – The most awkward plug on the locomotive – the
center siphon tube plug on the firebox front wrapper plate. The object
in front of the plug is the clamp bolt for the rearmost stainless steel
boiler band
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W02 – Trying out a tube socket for fit.
This example is an unusually long one, but you can clearly see the
restrictive 90 degree spacing of the bores in the drive barrel.
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W03 – Shaun Ackerman and Phillip Maurer (Right) are
crammed in between the rear driver axle, the fire box, the walkway steps,
the test coupling and the plumbing.
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A Tommy bar was duly found, with the usual
engineering pay-off (aka … conflict) between the long length for good leverage,
versus the access. Because of the cramped spacing around the rear drivers of
this engine (Pic W03 above), only one person could get a good grip. These
boiler washout and other plugs usually have shallow heads in relation to the
size of the square, so, even with one person putting all their strength into
holding the tube socket n place, if you tilt the Tommy bar, off it comes.
Reefsteamers are nothing if not inventive,
and the block n’ tackle was soon brought out. Dawie Viljoen was dispatched
to find a boiler tube to fit over the Tommy bar, and the tackle’s hook was
put into the open end (Pic W04 below), while the hoist hook was hooked around
a gwala bar wedged through the frames. (Pic W05 below) It took a while to
untangle the chains but they got the contraption set up. Phillip is a
natural with dangling chains, for, working as an electric freight driver in
Switzerland, surely he’s had ample experience in resetting the chains on Swiss
cuckoo clocks?
The hoist set-up was a failure. We were
able to put several fellows on the hoist chain, although only one at a time
could apply his weight while the others were restricted to biceps power only.
But with the leverage, the boiler tube just bent in the middle with a loud
pop and the siphon tube plug was as stubborn as ever. And it put up another
bit of a fight after a minute or two of discussion. Phillip was squatting on
his hams when the stowed hoist slipped and the hook set came down and bopped
him right on the head. His mandatory Reefsteamers hard hat saved him from no
more than a shock – but it was a graphic illustration of how quickly an
accident can happen in this rather rough environment.
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W04 – Rube Goldberg was a Reefsteamer! The chain
tackle is hanging from the boiler tube (in Shaun’s clasped left hand) while
Phillip looks for the right chain to retract the hoist – much to Shaun’s
amusement.
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W05 – Here’s the other end hooked onto a bar wedged
through under the driver axle bearing. All of this just to get one nut
loose!
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W06 – Take that! The stubborn Siphon Tube Plug get the
heat treatment to expand
it and to break the grip of the threads.
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Well, we were bending boiler tubes and
couldn’t fit any longer Tommy bars. The weapon of last resort was brought
out, the infamous acetylene torch. With the tube sockets, Tommy bars and
chief engineers cleared away from between the frames, the torch was played
onto that siphon tube plug from the left side of the engine. (Because
there’s a better walkway that side and it’s easier to trundle the heavy
cylinder trolley there.) It was quite a reach, you can see Shaun working at
full length, and wrong armed in Pic W06, but luckily with a convenient spring
upon which to rest and steady himself. Compactly built Andrew ‘Noddy’ King
was able to fit in the gap between the frames – by squatting on top of the
brake rodding, but the rest of us are too tall to do this with safety, with a
hot flame close by.
With the plug just starting to glow, it
was quenched with cold hose water to quickly contract it. It made a lot of
steam, which looked eerie wafting up from under the boiler barrel. (Pic W07
and W08) As it turned out, it only needed one heating cycle to crack the
‘grip’. The guys needed to put a Tommy bar and a tube socket back on. They
went for a shorter tube socket this time, but this meant that the stainless
steel boiler band had to be loosened slightly and knocked forward to clear
the work space. (Pic W09 below)
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W07 – The only time that steam emission is welcome in
this area. The siphon tube plug is being quenched to contract and loosen it.
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W08 – Howzat! The camera shutter speed froze the water
drops in space during a generous application of cooling water. Of course,
the boiler packing got soaked.
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W09– Wrestling to the get the boiler
band clip wriggled forward to clear
the way for a tube socket.
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But this was the end of the battle and the
stupid plug came out slowly with a 2 foot Tommy bar fed in alternatively from
either side of the engine to get enough swing in under the boiler barrel and
over the frames. You can see the mark of success in Pic W10 below. Andrew
got on with cleaning the plug before running the thread clear with a tapered
die. The initial scale came off with the wire brush wheel. (Pic W11 below)
Andrew eventually scraped out the valley corrosion with a chasing tool. (Pic
W12 below) This gritty stuff would have come out with a taper tap – but
would be likely to jam and cause wear in both the work piece and the tap.
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W10 – A simple hole that is the result
of a lot of work. The threads need to be cleaned and treated before
reassembly.
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W11 – Another fast shutter photo that froze the wire
wheel. The washout plug looked as if it was coming up clean, but some
corrosion still remained in the thread valleys.
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W12 – Close up of the tapered plug clamped in the vice
for deep thread cleaning. You can see the curved
taper-wear in the lower edge.
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The boiler has been under work for four weeks
to get it to this stage, including some week-day button-up work courtesy of
the pensioners. When prepping a steam locomotive boiler for a boiler test,
one has to either remove or block up any of the typical leak points as not to
cause an incidental drop in the test gauge pressure. Aiden Mc. Carthy, with
some assistance from Lee Gates, conducted the first boiler test. The first
job is always to remove one of the foundation ring washout plugs let the
residual water drain from the boiler, and insert the test coupling. This in
an interesting contraption as it uses a bleed valve to help modulate the
pressure. (Pic W13 below) Under conditions of high pressure and low water flow,
the throttling effect of a valve is much reduced. The main valve is a plug valve,
which isn’t a good design for throttling anyway. The bleed valve is a gate
valve.
This Class 15F’s boiler had already been
prepared for testing by the pensioners (who we call ‘The Spoories’) crews
during the weeks. Both of the water gauge columns had been removed and
blanked off. All three safety valves had been removed and blanked. The two blow
down valves were positively sealed with a plate-backed rubber plate and the
regulator’s (‘Throttle’) four multi-valves and the pilot valve were all ground
in and temporarily sealed. The ‘Turret Valve’, the steam locomotive’s ‘main
switch’ for all the steam operated equipment, was also ground in and shut
down tight within the turret manifold.
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W13 – A general view of the test coupling which clearly
shows the locomotive-sourced gauge, the plug type main valve and the red-handled
gate valved bleeder
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W14 – Even with the use of a fire main, Aidan Mc.
Carthy has to sit patiently while the boiler tops up. He’s actually
sitting on the rear jacking block of the Class 15CA ,which was still
waiting for her front bogie on this day.
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W15 – A rare view of a blanked off safety valve pad.
This is the vent pipe to allow
the displaced air to leave the boiler. That’s the valve that caused some
confusion.
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We had a conveniently located and
functioning fire hydrant to top the empty boiler up – rather than wasting
half a day filling up the boiler with a conventional hose pipe running
through an open washout plug. Even so, Aiden had to sit and wait for the metallic,
echoing splashing to stop, while I buggered off with the camera to catch pics
of the other work teams doing their stuff. (Pic W14 above) We can tell that
the boiler is full when water starts running from the overflow pipe that runs
from the safety valve pads. There was some confusion with the plug type vent
valve at the head of the vent pipe. (Pic W15 above) It works opposite to
the usual standard – the valve is open with the handle 90 degrees to the
pipe. (Normally this indicates the valve is closed.) The first test up to
water mains pressure was a failure. I couldn’t hear anything (Only having
effective 35-40% hearing and my stupid 24/7 tinnitus often sounds like a
mixture of escaping steam and the staccato hissing of a clapped-out surface
discharge toilet cistern topping off – which masks any hissing I might have
heard), but Aiden could clearly hear water squirting somewhere under pressure
– exactly what one DOESN’T want to hear when pressurizing a boiler. It turns
out that the boiler wash-out crew hadn’t fully tightened up the washout and
siphon tube plugs in the back plate and water was squirting right through
into the cab.
Bad Spoories!
Well, if one plug is loose, they probably
all are. Aiden and myself worked patiently all around the cab and the
firebox, tightening up the plugs. But we had a problem in that the boiler
surfaces, the cladding and the packing were already well soaked from our
premature failed test and it would be hard to see any genuine new leaks after
the plugs had been properly tightened. And a cold boiler takes a while to
dry off. We conducted three water mains pressure tests during the day and
although there was an improvement in the ability of the boiler to retain
pressure, the boiler couldn’t hold the kPA. The left hand clack started
leaking with the slightly higher pressure and had to be ground in, as well as
the take-off valve (Pic W18). The center siphon tube plug on the front
wrapper plate was known to be leaking, and there was an unseen leak in the
upper left firebox, possibly under the cladding. That’s bad news as it
usually means that a boiler stay has broken, or a stay rivet has corroded.
But as everything was already wet or damp, it was hard to tell for sure.
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W16 – Lee tightens up a plug in the cab back plate.
This one was dry but they all got nipped up anyway. ‘Gerda’s’ dark
blue paint shows up well in the flash.
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W17 – A siphon tube plug that’s weeping
just above the stoker jet manifold. Steam locomotive cabs abound in brass
obstacles especially designed to hinder the use of Tommy bars
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W18 – The take off valve starts to leak during the 2nd
test at a higher pressure after all the washout plugs have been tightened
up.
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Lee Gates and Andrew King did the next
round of boiler tests two weeks later. The water mains pressure, which is
quite variable at out depot, was reasonably good today and we got the boiler
up to 1000Kpa on occasion. Nothing went bang. We focused on the boiler
itself, which had dried out over the two previous weeks, and Lee was put to
the task of getting the boiler properly buttoned up while Andrew used both
his eyes and his ears to check for leakage. Andrew uses a piece of chalk to
mark a cross on suspect plugs and that cross is only eventually removed once
the plug is certified dry and non-leaking. Most of the boiler plugs are
fairly easy, but the three plugs on the under belly are two man jobs as one
fellow needs to hold the tube socket. If you drop it, it falls right through
the frames and into the inspection pit ... a real schlep to have to duck-walk
under the engine every time you drop the works! The various cab plugs were
dry but we nipped them up ’for luck’ anyway.
Three stubborn leaks were found up on top.
The washout plug right behind the safety valve mounting pad just wouldn’t
stop weeping. A rivet was leaking under the right front safety valve and the
pressure gauge shut-off valve was leaking through the gland. (The pressure
gauge has its own valve so it still indicates boiler pressure even when the
turret is shut down.)
The safety valve pad leak was solved over
several sessions of judicious tapping with a flat ended drift, to peen the large
recessed rivet over into its gap. The washout plug was another story. Even
after tightening up it still wept. We even used PFTE plumbers tape on the
taper to try and prevent the water creeping up the threads. It helped, but
we still had a stubborn bubbling. The pressure gauge shutoff valve was a
problem too, with the leak worsening under tightening of the gland nut. But
we just knocked the valve all the way shut and the leak stopped. Good enough
for a boiler test but one has to remember to switch it back on again! It’s
surprisingly comfy sitting cross legged up on top of the boiler, with the
turret manifold to your back and the safety valve pads to the front, and the
characteristic insulated turret feed pipes very conveniently one to either
side for foot rests or hand holds.
The water mains pressure suddenly failed
in the afternoon (I won’t repeat Andrew’s swear words) and the pressurized
boiler started discharging back into the water mains during the afternoon
test. So we coupled up the WAP pump and got the boiler up to 1600kPA and
holding. It still leaked very slightly, but that was known and estimated to
be the siphon tube plug on the front wrapper plate (featured in the article)
so we’d made progress.
On the day following the removal and
replacement of the stubborn siphon tube plug, the boiler was buttoned back up
and run up to the 125% operating pressure as required for boiler testing. No
leaks were found. The boiler was officially hydraulically tested and passed
on that score – but the visual inspection came up with some potential
problems. The back firebox corners are suspect – but they will be closely
examined and ultra-sounded to check for thickness within a week. While the
inspector is present, the front corners and the throat plate will be checked
as well. If we have to take the engine out of service to fix the firebox, so
be it – but it means she won’t be running for the Free State Explorer.
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SIA PROJECT : Class 15F No.3052 ‘Avril’ Reverser Repair
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FP03 – A tired old lady who made it to her destination
in spite
of mechanical issues and poor coal. Fundamentally, Class 15F No.3052 ‘Avril’
is a good runner and has a great rate of steaming.
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Aidan Mc. Carthy got assigned to this one,
a quiet job working by all by himself in the Top Shed. Those who are
following our (mis)adventures will remember that we ran Class 15F No.3052
‘Avril’ for her first revenue earning trip for Steam in Action three weeks
ago. She ran very well, as allowed by the deadly combination of poor quality
coal and a failed grate shaker. But a number of problems became apparent. The
power reverser was one of those problems– as it lost much of its damping oil
on the Magaliesburg run and had to be refilled several times. We knew it was
leaking but the severity of the leak surprised us once we were out on the
line.
But first, a bit of background. The typical
SAR power reverser is basically a steam-powered linear servo motor with
damping and a hydraulic lock mechanism. It consists of a pair of cylinders (of
equal ‘stroke’, or length) which are linked together by a common piston rod.
One cylinder (front) is a steam cylinder that contains a double acting steam
piston that can have steam applied to either one of its faces to move it to
one end or the other to power-shift the valve motion. It is directly connected
to a similarly sized ‘lock’ cylinder that is totally full of oil at both ends.
Both ends of the lock cylinder’s cylinder are connected by what is known as a
‘cataract valve’. As the power cylinder’s piston moves, the common piston
rod moves, which tries to push or pull the lock cylinder’s piston through the
oil. With the resulting pumping action, the oil is bled from one end of the
lock cylinder to the other means of the open centrally-mounted ‘Cataract Valve.’
The restriction of the viscous oil flow through the valve’s ports acts as a
drag on the power cylinder and slows the valve motion movement down to a
controllable speed. It’s a similar methodology to a car’s spring damper, or
a traditional hydraulic door closer. If the centrally mounted ‘Cataract Valve’
is closed – no oil can flow from either end of the lock cylinder to the
other. The incompressible oil trapped on both sides of the lock cylinder’s
buckets hold its piston rigidly in place, which, via the common piston rod, holds
the power cylinder’s piston in the desired position, and thus keeps the
locomotive in the correct selected cut-off. (or ‘gear’)
R00 – A general
layout of a ‘Hadfield’ reverser with the front of the locomotive to the
right. The green cylinder is the hydraulic lock cylinder, crowned by the
cataract valve. The red cylinder is the double ended power cylinder, topped
by the black steam valve, the thin live-steam supply line coming in from the
right, and the cylindrical brass displacement lubricator on top. The long
red bar is the front reverser lever, while the long green bar is the
indicator lever that operates the pointer on the reverser quadrant, back in
the cab. Notice the two cylinders are coupled together by a common rod. The
leak was at the extreme left, behind the copper boiler feed pipe
Without a functioning lock cylinder, ‘Avril’s’
power reverser kept creeping to full forward gear. (Equivalent to 1st
gear in a road vehicle) The actuating (power) cylinder, without the braking
and damping effect of the oil within the lock cylinder, reacted too fast and
kept over-shooting the driver’s cut-off settings. In fact it tended to slam
to either full forward or full reverse with little control in-between. The
crew had a very interesting run to and from Magaliesburg!
And the poor old engine ended up in a bit
of a mess. (Pic R01 below) I spoke of this as being a ‘debut run’. ‘Avril’
reminded me of a matriculant school girl, who’s spent hours getting all
dolled up for her graduation dance … only to spill a big sloppy chocolate
cream éclair down her beautiful silken gown, on her big night.
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R01 – ‘Avril’ needs a bath with a right mess to have on
the running board after a debut run. You can see the green ‘valve oil’
running all the way past the left frame
of the photo.
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R02 – The lock cylinder’s rear cylinder cover has been
removed but is being blocked by the RHS boiler feed pipe. Notice the air-bleed
bolt in the top of the cylinder.
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R03 – Aidan Mc. Carthy looks still reasonably cheerful
(and clean) as he loosens the feed pipe nut. I thought it would be prudent
not to show the picture of the mallet and ‘slogging spanner’
in enthusiastic use!
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Chief Engineer Andrew King already had his
suspicions about the cause of the leak, which turned out to be 100% on the
money – but there was also another unexpected problem uncovered, which even
his magnificent mind didn’t come up with. Aiden Mc. Carthy’s job started
simply enough with unbolting the end of the cylinder with car-sized ring
spanners. That glistening green oil left over from the trip amply
demonstrates the logic behind the SAR tradition of painting the lock
cylinders and the indicator linkages green – it matches! (Although, you can
see by the worn paint that No.3052 ‘Avril’s’ lock-linkages were originally
painted blue.)
Because the end of the piston rod isn’t
belled or obstructed, it wasn’t necessary to dismantle the glands or the
seals to get the assembly off. You can see the cover half-pulled in Pic R02
above. This was Aidan’s first challenge of the day, as the cover wouldn’t
come off past the wide bore boiler feed pipe. This is one of the two
characteristic diagonal copper pipes that one sees climbing up the sides of
the boiler to top-mounted clack valves on nearly every SAR steam locomotive.
And the lower bend (Pic R02 above) was in the way.
This seems like bad design (and it is) –
and it actually is more a result of standardized placements being mixed with
part-placement unique to a class of locomotive. But normally the lock
cylinder’s cover doesn’t have to be removed to change the seals. Remember
that we didn’t know for sure what was causing the leak so everything had to
come off. Aiden had to do a bit of ‘slogging’ with a mallet against a round
handled ‘slogging’ spanner to ‘break off’ the over-sized nut before using the
spanner manually. (Pic R03 above) We could hear him from the club house!
Aidan then loosened the top nut at the clack valve and tried to rotate the
pipe to get the bend. It was close, but as often happens with steam locomotives,
‘close’ just isn’t good enough. The boiler feed pipe had to come off and Andrew
King was called in to help with the removal. The pipe actually ‘popped’ out
of the clack valve with a bit of 2 foot crowbar action. (It was a LOT harder
to get it back in again.)
They then dismantled the valve packing and
Andrew’s original suspicion was proved. There’s a brass bush at the outer
end of the seal stack and it is usually machined tapered for an asbestos rope
seal and flat for more modern ‘Chevron’ seals. We had the older style
tapered bush running with new seals. But the surprise problem was that the seals
themselves had been installed back to front. Most bearing and shaft seals
run with the smooth or convex side facing the medium to be sealed, and the
grooved or concave side facing the external area. Chevron seals work the
opposite way – and it would be natural, if one doesn’t know any better, to
place them rounded ends facing the entrained oil. Chevron seals use a
tapered outer ring which is quite flexible. As the pressure builds up behind
the seal, the oil pushes against the concave side, behind the chevron. The
effect is like holding an umbrella upside down and filling it with water –
the dome of the umbrella will tend to become wider in diameter. The angled
chevron thus tries to straighten out and the effect is that the seal expands
in diameter and creates a tighter seal when under pressure. There are 5
seals in this pack, each one sealing the bit of leakage from the one behind
it.
But if the seals placed back to front, as
these were, the pressure of the oil closes the outer angled ring, closing the
chevron and making the seal effectively smaller in diameter. The oil leaks
past the bearings with ease. With a slight vacuum in the cylinder now, if
the piston moves the other way, the chevrons open up with atmospheric
pressure and block the leaked oil moving back into the cylinder from the
gland packing cavities. In effect, the reversed chevron seals act like the
one-way valves in a very slow pump. The engine literally and positively pumps
oil from the lock cylinder every time the reverser lever is operated and
returned.
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R04 – A set of new lock cylinder ‘chevron’ seals.
These are in two stacks of five.
The top, domed surface, faces the atmosphere which the inset folded
undersides face the oil chambers.
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R05 – A view up inside the cylinder. You can see the
green bell crank to the right of the cataract valve – which relays the
motion from the power actuator. Note the cylinder head gasket had broken
upon dismantling.
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R06 – This is the tapered outer bush
being set up and centred in the lathe to cut the seal surface down to a
flat plane.
The problematic taper is visible in the light reflections to the bottom of
the picture
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The outer seals in the stack had been
damaged by running backwards against the taped bush. The new seals come in
sets of five (Pic R04 above) and it is false economy to change just one or
two of the disks. So the entire set was replaced. They were found to be too
large in diameter and had to have slots very carefully cut out of them. The
gap had to be such that it would close up with a very slight overhang within
the gland cavity – with no leaks, but also with minimal overlap as not to
affect the operation of the neighbouring valve rings.
James Thomson was put to the task of
machining the outer bush flat, to suit the new chevron seals. (Pic R06
above.) After centering the bush in the chuck, the entire job only took him
a few minutes, as the length of the bush isn’t critical. (It is pulled down
by the gland packing cap anyway.) The gland packing cap was found to be a
bit bent, so James and Juan had a go a flattening it in the 50 ton press.
(Pic R07 below) They weren’t successful so they tried to spring the plate
straight with a bit of mallet action. Juan ‘Nippies’ Buys looked as skeptical
as I felt (Pic R08 below), but he managed to spring the plate out somewhat
straighter.
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R07 – The gland cap in the 50 tonne press.
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R08 – A sceptical looking Juan “Nippies’ Buys prepares
take a lusty swing at the
gland cover clamped tightly in the vice.
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R09 – Some heavy duty arts and crafts
time. James is cutting out a donut shaped gasket for the lock cylinder
cover.
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James Thompson then got busy cutting out
the gasket material with a heavy duty pair of tin snips. (Pic R09 above) We
needed a new gasket for the lock cylinder’s end cover as the old one broke
apart upon removal. We Reefsteamers generally replace or re-fabricate
gaskets upon removal anyway, and copper ring gaskets are re-annealed as a
workshop standard. The blades on the first pair of snips kept spreading on
the pivot as this material is tough, impregnated fibre-based sheet and isn’t
rubber as it appears. The inner and outer edges of the gasket were trimmed
with the snips instead of the hammer, as we normally do,, as the inner raised
surface is too shallow to present a decent corner with which to tap-cut the
gasket. But the holes were easily accessible to the ball peen (Pic R10
below) and James got to use his tapered awl too, making a really neat job of
those holes.
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R10 – Classic ball-peen hammer action to make the holes
in the gasket. Notice the
awl-like punch in James’ left hand – he did a neat job of punching the
holes out.
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R11 – Here is the seal assembly and the two bushes.
The top bush is the ‘top hat’ that fits into the cylinder cover, while the
lower bush is the tapered bush that was machined. Notice the slots cut
into the new seals.
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R12 – Putting the cover back on. Positioning the cover
was easy as the gland nuts lie horizontal and the side with the most green
paint remaining faces outboard.
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With the gasket prepared and ready, Aiden
wiped out the inside of the cylinder and scraped the dead gasket from the
sealing surfaces. The cover went back on easily and with care to tighten the
nuts in diagonal sequence. (Pic R12 above) Aiden used a 26mm spanner, which
is a miniature nut by steam locomotive standards. The inner ‘top-hat’ bush
is already in place in Pic R12, and the seals were assembled after the cover
was tightened. Each individual seal had to be rotated to stagger the slots
and its edges carefully fed into the bore to prevent crimping and tearing. With
the gland cover loosely snugged up, two seals were still outside their cavity.
(Pic R13 below) Aiden had to take a lot of care to get those seals in
straight and untorn.
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R13 – Half compressed seals in the loose gland
assembly. Notice the angled gaps. The seals are now sitting flat against
the newly faced brass bush.
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R14 – A bit of gentle persuasion to get the boiler feed
pipe back into its sockets. Out of the photo, Aiden is simultaneously
levering at the lower bend and both gentlemen are assiduously seeking the
magic angle.
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The seals and the cover went back on with
little trouble, but the boiler feed pipe was another story altogether. A 2 ½
inch copper pipe is surprisingly unyielding! After various combinations of
Lee, Aiden and Andrew trying to get that pipe in – we sourced two crow bars
and levered the pipe simultaneously at both ends. (Pic R14 above) It was
quite a wrestle but eventually the magic angle was discovered and the stupid
pipe just popped straight back in. The cylinder was left empty but will undergo
testing at the next boil-up, especially as the seals may need to be nipped up
a bit more once they’re under pressure.
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SIA PROJECT : GMAM Garratt No.4079 ‘Lyndie Lou’ Stoker
rebuild : Tested!!
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S01 – An assembled GMAM Stoker Motor awaits testing
under compressed air.
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I wasn’t at the depot on Sunday, (Had
office work to do at home … bleh!) A small team of Reefsteamers were at
work, putting the front end of the Class 15CA together, and checking out the
GMAM stoker. The crankcase was refilled with heavy weight motor oil (20W 50)
as for older car engines. The intake ducting was hooked up to compressed air
and the motor run under pressure. The newly overhauled two cylinder double
acting steam engine is reported as running very smoothly. It has been passed
for refitting into the waiting arms of the big green machine that is bolted
between the two brass ‘Lyndie Lou’ nameplates.
The test team members were careful to
lubricate the engine with MH oil poured through the intake before starting up
with compressed air. (Only the crankshaft, its bearings, the big ends and
the valve eccentrics are lubricated by the entrained oil – the valve spindles
and the pistons are lubricated by steam-bourne oil.) A bench tested
mechanical stoker motor has the same problem as a dead steam engine in tow –
the hydrostatic lubrication system isn’t available A mechanically lubricated
locomotive, such as our Class 25NC and the Sandstone Estates GMAM Garrett,
has an easier time of it as the mechanic rods are still worked from the
eccentric crank. But in cold temperatures, the oil would tend to gel in the
tank and not feed into the pump’s cylinders.
Our focus now is on getting our
mechanically stoked Class 15F’s (No.3016 Gerda’ and No. 3052 ‘Avril’) in
tip-top condition for our coming tour. But the new axle bearings and the
overhauled stoker motor are ready and waiting to go into the Garratt.
Shaun Ackerman is pleased with the work
and this is what he has to say….
The mechanical stoker engine is brand new
and will run well for many years to come,
once again the quality work that Reefsteamers and its members deliver all the
time.
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PROJECT : Coach Repairs
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Coach work continued with Fred Sewell doing
the electrical work, and our two coach restorers keeping themselves very busy
in the kitchen of No.42, the Management Car, as well as hanging pictures in
the bar car. Meanwhile, the Mathee and Son axle greasing team were on the
job.
Fred’s coach work was the opening and the
stripping of the old light fittings within the compartments of the Sleeper
Coach No.23345. The old lamps were actually intact and working, but were low
voltage units running from heavy transformers stashed in the incomer panels.
As mentioned previously, the coaches are through wired for 220V, primarily
for the water pumps, bar car and kitchen fixtures. Now the lamps are
gradually being wired to run from the mains voltage as well. One feature
that will unfortunately be hard to replicate are the low wattage night lights
that are fitted to the sleeper lamps. (Pic C01 below)
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C01 – An original 110V coach lamp that had been retro-
fitted with 600mm long 24V tubes (to no longer require an inverter) is
resting on a coupe’s table. It is now to be modified (for the last time)
with 220V electrics. What looks like two long thumb screws between the
tubes are the low-wattage incandescent night lights.
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C02 – The Wehmeyer Bros. Coach Restoration Specialists
are working out of sight between the rolling stock in the coach yard. That’s
Willie on the left and Lex on the right. That’s about half the tool kit
that they brought today.
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C03 – A unique hand-made drawing
of a Class 15F done with hot wire and soldering iron work. It’s great to
have
this drawing (dated 2003) finally riding the rails.
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Fred Sewell had a rough day of it, working
in a hot coach with nary a breeze wafting through the windows. He was in
pain too, his recent kidney tumour operation site playing up after getting
pulled from sitting too long during the week – and he wasn’t able to last the
entire day. However, we have another coach that is switching over to the
reliable and brighter 200V supply, eliminating troublesome transformers and
inverters.
The Wehmeyer brothers started their day
with the usual latch, handle and hinge work. But you could tell by the
spread of tools laid out in the walkways that they had something more
involved in their collective minds. (Pic C02 above) The more involved work
was that of mounting pictures on the paneled wall behind the bar. We’ve already
had decorative stuff up there – but jokey, bar room type gimmicks and wanted
to put up something more classy and railway themed. Furthermore, the
original décor script was in Afrikaans, which our overseas friends (especially
SIA members) wouldn’t understand. The new locomotive themed decor, pictures without
words, is a language that any steel-wheel buff can understand! The boys did
well today, not only putting up dignified collection of art work in the bar
car – but selecting and putting up pieces that are hand crafted, signed and which
are unique pieces in their own right.
A set of soldering iron branded drawings
of locomotives were finally put up after hanging around in the club house and
at risk of being damaged. (Pic C03 above) A special piece made in leather
takes pride of place at the end of the bar. (Pic C04 below) It is the last
work by a recently deceased friend of the Reefsteamers and a lover of steam.
It’s appropriate that we can remember him every time we relax in the bar car
or proceed through on Coach Controller or Train Management duties.
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C04 – A handcrafted Class 25NC printed
and stained onto stretched leather.
This is a special sentimental piece for
us Reefsteamers as it is the last (and incomplete) work of the late Dewalt,
husband of Lenie, of Angel Tours.
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C05 – A rarely photographed Lex Wehmeyer does his stuff
with a power
screw driver. He did a brilliant job as
the piece hangs straight with none of the fixings visible. (See Pic 04)
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C06 – The bar looks great and very dignified with its
new railway themed art pieces.
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Lex Wehmeyer put the hangars and brackets
on the pictures – enjoying the use of an electric screwdriver. (Pic C05
above.) He did the hangars of the soldering iron drawings by hand, as their
frames are more brittle. You can see the finished result in Pic C06 above.
An unexpected bonus of using these art pieces was that the black, brown and
red colours blend in perfectly with the décor.
The big coaching project of the day was to
refit shelving in the refrigerator cavity of the management Coach No.42.
This coach is essentially a self contained motor home on flanged wheels. It
was originally kitted out with a fully fitted kitchen, including a built in,
heavy duty refrigerator in one corner. (Pic C07 below) The refrigeration
equipment is 110 volts and is unusable. Only one of the original stainless
steel shelves survived, as well as a group of wooden drawers. It was decided
to replicate those shelves in wood and to remount the doors, to convert the
refrigerator cavity into a cupboard, which, incidentally, will still benefit
from the original insulation. The original doors are very thick and heavy,
being of solid wood block construction. (Pic C08 below) Finding hinges to
fit the deeply inset recesses of the stainless steel frame is a future
challenge, as the repair job will need to be strong enough to support all
that wood. (Pic C09 Below.)
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C07 – The original fridge cavity in the corner of the Management
Coach’s kitchen.
The blue curtains cover the gangway door windows and the stainless steel
fridge to the left is a 220V commercial upright unit.
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C08 – A solid, heavy 9cm thick wooden
door to be re-fitted to the fridge cavity.
The insulation will still be useful even
if the refrigeration no longer works.
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C09 – A future cabinet making
challenge – deeply inset hinge
recesses in a stainless steel frame.
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The shelving work started, as many jobs do
at the depot, with a good ol’ scrounge. Willie found some nice piece of
laminated board in the old fitting shed, and it was conveniently laid out on
a central table (hence, still flat) and accessible too. Lex and Willie had
actually brought their own shelving boards to the depot but the material was
too short for the refrigerator cavity. (Pic C10 below) Something that
complicated the job is that the back panel of the refrigerator cavity isn’t
parallel to the front. It actually tapers inwards, following the vestibule
line, as the refrigerator occupies the space normally taken by a coach door.
Rectangular shelving would work, with extra deep brackets at the back, and an
inevitable gap – but that’s an ugly solution which is anathema to the
Wehmeyer Bros. Willie laid out the stainless steel shelf on the generously
sized boards and marked the outlines, for cutting with a jig saw. (Pic C11
below) Lex did the sanding and planing in the shade of the ‘Tea Tree’ in the
middle of the ‘The Green’. (Pic C12 below) No splinters for these boys!
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C10 – Willie checks out the original stainless steel
shelf as a template. Note the brought boards leaning against the coach.
The day is moving on and the shade is expanding.
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C11 – The fridge shelf laid out on the boards. Notice
that the front face (bottom) is not parallel to the rear face. The rear of
the fridge cavity follows the angled line of a standard coach vestibule
door way.
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C12 – Lex Wehmeyer at work cleaning and bevelling the
edges of the raw cut shelving. That’s the No.42 Management Coach in the
background, with the unique wide framed windows.
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The original mounting stainless steel mounting
hardware is still intact, including the shelf supports and the front braces.
It just needed some gentle straightening and loose or missing fasteners to be
repaired. (Pic C13 below) It took some extra work to this. But it means
that should we be fortunate to find more original stainless steel shelves
from a matching coach – they can be retro-fitted with little trouble. Fitting
the shelves went with little problem, but the brothers soon came against the
snag of the old fridge walls not being truly vertical. Those carefully cut shelves
are slightly too small for the cavity, but still mount well enough within the
cavity. The bare wooden surface needs to be varnished or sealed before being
used for food, but the new shelving is already coming in useful to get the
fridge drawers off the blue and white floor and safely out of the way! (Pic
C14 below) The brothers managed to get two wooden shelves in place (Pic C15
below), and the stainless steel shelf is back in its place again. There are
two more shelves to be made and then the doors need to be re-hung.
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C13 – Willie Wehmeyer is refitting the original
mounting hardware. It was painful exercise. Notice that he’s resting on
his shin bones against the sill rail and his thighs are bound by the
original front brace.
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C14 – As much a heritage piece as a steam locomotive –
One of three matching original SAR wooden fridge trays, with original
interior finish and intact front panel.
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C15 – The old fridge cavity is becoming more useful
again, with two new shelves installed and the original back in its place
again.
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Occasionally, during the tapping and light
hammering work, a out-of beat, counterpoised hammering could be heard echoing
in the coach lines. It was a reminder that the coach running gear team were
at work, greasing axle bearings and replacing a set of brake shoes. Andreas
Mathee handled the bearing job – doing it unsupervised now that he’s done it
a few times with his dad. (Pic C16 below) Andreas is also checking the
stretcher beams and the horn guides, and is picking up techniques for the
brake rigging work. Cliffie Mathee and Tony King were both at work on coach No.137
and changing out the original spec cast iron brake shoes for modern
composites. (Pic C17 below) It might sound odd, especially with all the
fuss we hear about high performance brake pads for cars, but plain cats iron
is one of the best braking materials against a steel wheel. But they are
antisocial in that they squeal, chatter and throw sparks. That’s neither
here or there in our 21st century context as the old cast iron
shoes are no longer being manufactured. The composite shoes are less likely
to draw sparks, but have a lower friction coefficient. Cliffie is fretting
about the ever decreasing supply of brake shoes – and in his authority as the
Reefsteamers Safety Officer, he can pull a coach out of service. With the
distances and speeds that we run, | |