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Reefsteamers Depot News
Report
- 12 - 19 JULY 2008 -
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INTRODUCTION :
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Two weeks ago was a cold, grey,
overcast day – where most sensible people sneak a few extra hours in
bed. Of course, we aren’t all that sensible and were happily
pottering around the chilly, gloomy depot. The day started off
slow. You could see people were still spooling up. But it
turned out to be a productive day with our people working in the
workshop, amongst the coaches and on the fencing lines.
The photographs from that day
aren’t that good – but at least you don’t get such harsh
shadows.
Last week was a pleasant day at
a very busy depot. We basically had 5 teams at work.
Hunslet Taylor Strip-down, perimeter fence gate fabrication, Class
12AR boiler tube preparation + installation, Electrical repairs and
rehabilitation work on the ex-Sandstone Coaches. Scrap recovery
company, Reclam, was on the premises finishing up the cutting job on
the burnt out Transnet couches out back – and the Sitemela
Contractors were hard at work. I was buzzing around like a
blue-arsed fly trying to keep up with everyone. The photographer
probably walks more than any other person at the depot when everyone
is so spread out.
But isn’t it so much better
to hear of a live, busy Steam Depot than of a stripped, derelict
depot, up to the window sills in weeds and the gaunt leaf-drifted
remains of locomotives sinking into the ground under knarled tress?
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PROJECT – Booth Crane No.96 - Cleaning a
Steam Crane’s Boiler :
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Patrick Ackerman and Dawie
‘Swak Hart’ Viljoen were the two boiler boys today. (Two
weeks ago) Patrick arrived at normal Depot working hours and had
come with a secret weapon. He had his own brand new needle gun,
in flawless satin black finish and stainless steel. (Pic B01
below) He had also come fully equipped with his own hoses, hose
couplings and a filter + moisture separator set for the air
compressor’s lines. Our air compressor plant has little
filtration on the intakes and the entire system is very prone to
condensation – which would mess up a pneumatic power tool fairly
quickly. This is true even when we blow out the lines to
atmosphere upon the first opening of the valves. The filter and
separator set fitted against the air-line’s I-beam column after some
juggling of nuts and fasteners, as it could not be rotated around its
axis.
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B00 – A steam age exfoliation.
Patrick and Dawie patiently spend
their entire depot day cleaning this vertical flue water tube
boiler – of
which only three of this particular model are known to have
survived.
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David Jacobus Viljoen sneaked
in later – obviously after a late night of carousing and chasing
girls. Actually, Dawie lives in Potchefstroom, a university town
that is just CRAWLING with girl students, but is 1 ½ hour drive away
from the depot. The two of them got stuck into their all-day
task of de-scaling and de rusting the boiler. Patrick operated
the needle gun – with great gusto (Pic B02 below) as he was enjoying
operating a decent functioning power tool for his second round.
He was concentrating on the rivet heads, seams and the flanges while
Mr. ‘Swak Hart’ got stuck with the rotary wire brush and got the
loose powdery stuff off. (Pic B03 below)
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B01 – A workman is as good as his
tools,
or something like that. After wasting time
with asthmatic air tools last week, Patrick Ackerman brought
in his own equipment.
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B02 – Pneumatic and dangerous – a
grim
looking Patrick tackles one of hundreds of
rivets to be cleaned this day. Notice the full
safety gear, goggles, ear muffs and gloves.
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B03 – Dawie tackles the looser stuff
–
although the really loose stuff and
the flaky remains of the insulation
were removed the previous week.
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The boiler’s grate and fire
bars had been removed during the week and had been placed in their
relevant positions on the workshop slab. (Pic B04 below)
No abnormal wear was found. The grate was found to be in fairly
good condition, with the exception of a deep crack on one side of a
removable sow-bellied fire bar. (Pic B05 below) It isn’t
a crucial problem though, as it can be cleaned up and re-welded closed
again.
The Chief Engineer came poking
around later on and inspected the work, with close attention to the
flanges and a once over of the foundation ring. In this boiler,
once the two large oval shaped inspection hatches at the ends of the
two tube bundles are removed, you can stick your head in through the
holes (Pic B06 below) and you can actually look down into the water
space between the firebox \ flue assembly and the outer shell.
It’s not possible on a steam locomotive without using mirrors, or a
fiber optic type viewfinder – or by literally cutting away some of
the plating.
He pointed out potential weak
points and re-affirmed the issue of the pitting on the crown sheets.
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B04 – The circular fire grate assembly
with
the relevant positions and the position of
the seven central fire bars preserved.
For fire cleaning, the bars are hooked out by the cross
pieces visible between the slots.
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B05 – Lee points at a deep crack found
on one of the removable fire bars.
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B06 – Hello? Anyone in there?
The Chief Engineer takes a squiz at
the lower cluster of tubes. He was a
bit doubtful but confident enough to
allow the cleaning work to continue.
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We ended up in discussion about
the odd measurements used for the rivet hole spacings – as the
overlapping curved sections are drilled as flat plates. But the
holes drilled in the outer plates have to be fractionally further
apart than the corresponding holes on the inner plate, because the
plate’s final curvature is a higher radius. Some complicated
calculations there and when this boiler was made, calculators were
mechanical devices and slide-rules, no electronic aids and
computer-based drafting. <<Tips hat to those long ago
engineers and artisans.>> Andrew was confident enough to
let the young men continue with their cleaning work. Or, he just
wanted to keep them occupied and out of mischief. Anyway, the
cleaning work continued and the bolted-on firebox door frame and
assembly (Pic B07 below) was removed for cleaning, and for access to
the boiler shell behind it.
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B07 – The firebox door and frame just
before removal. If you look carefully, the
upper of the two nuts is already loose. Normally you’d
be able to see the grates
where you’re currently looking right
through the firebox.
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B08 – Your rust or your life!
The boiler bandit checks me out with a jaundiced eye as
I take a photo from a
perch up on high and safely out of range!
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B09 – An upper view of the boiler
descaling station - the symmetrical arrangement of the fire
hole, the water
gauge glass flanges and the pressure
gauge tapping is clear.
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Tony ‘Shakey’ King had a go
with Patrick’s descaler on the removed firebox door.
Meanwhile, Dawie moved around to the dark side of the boiler and found
that the rust was too much to handle. After blowing powdered
ferrous-oxide dust out of his nose, he rigged up a bandanna to
continue his work. (Pic B08 above)
I climbed up onto the empty and
still rust-piled boiler deck of the crane itself and took some detail
pictures of the crane for later use. Eventually I climbed up on
top of the water tank, standing astride the dynamo and took a rare
shot of the top of the boiler. (Pic B09 above) Doesn’t
so bad from this angle does it?
Our usual boiler inspector,
Dawie Olivier (From OSG) came by on Tuesday (15 July) and examined the
boiler. To our dismay, but not total surprise, he pronounced it
unfit to use. The pitted ‘crown sheet’ (Pic B11 below) and
the foundation rings are a problem, and there is evidence of metal
thinning around the firebox door. I must emphasize that this
boiler CAN be repaired. It’s just going to cost money and
mucho-time with the fabrication work to be done.
In the meantime, it is likely
to end up partially reassembled, the firebox doors put back, carefully
painted for weather proofing and put on static display around the new
formal club house. (Where it will keep the existing ornamental
smokebox door and the loco driving axle company on the lawns.)
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B10 – A half cleaned inspection cover
flange – the lower right quadrant has had the descaling
treatment. Visible within is one of the slanted flanks
of the flue, which we call the ‘Crown Sheet’, and the
external
pitting is visible.
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B11 – Up yer kilt! A view up
through
the firebox of the tipped boiler. The firebox
door is mid 10-11 o’clock. Under the
lower bundle of tubes, the sloped ‘Crown
Sheet’ can be seen (5 o’ clock) and the
external pitting thereon was a failure point.
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B12 – Check mate! The inspected
boiler lies in surrender on its side as
its future role is discussed. It might be painstakingly
weatherproofed and plinthed until future restoration when we
have time and manpower.
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There is another vertical flue
boiler at Millsite – but that’s a larger boiler for a 65 ton
crane. It is compatible with the Crowans Sheldon No.50 that is
standing against a set of buffers in open air storage. The
Sheldon crane, by the way, appears to be complete apart from the
boiler fittings, but due to long term storage in the open air, all the
bearings have rusted solid. Thus, the Booth Crane No.96
‘Shosholoza’ boiler rebuild project has been put back onto hold.
(Pic B12 above)
However, it is not the end of
the drive to get the Booth Crane back into steam. (Stubbornness
is a well known steam preservation trait!) Preliminary
discussions are under way to create tap-offs from one or two of our
locomotives, and to pipe locomotive boiler steam to the crane to
operate the crane’s power mechanisms. It would be a similar
concept to the old fashioned American Snow Plow (American spelling!),
where the rotating machinery in its own cabin was actually powered by
the locomotive pushing it.
Although the Booth Crane No.96
is actually self propelled, it has a mind blowing top speed of about
5kph and is safely operated at half that speed. The crane’s
propulsion system and gear train is designed for final positioning
rather than relocation – the work crew’s locomotive is required to
shift the crane and the accompanying job car around. So you’d
have an attending locomotive anyway. The Chief Engineer still
needs to approve of the concept.
The concept is sound as it’s
possible to procure high-pressure high-volume flexible steam piping,
which is basically flexible, reinforced piping with armouring.
Many of the large later model SAR locomotives already have a tap off
valve anyway. A valve could be fitted to any engine with very
careful positioning and attention to the flanging. These are
sometimes called ‘filler valves’ and were sometimes used to
pre-charge a locomotive’s boiler with steam and\or hot water to
speed up the time to get a cold locomotive in service. If we do
choose to fit a valve, the 15CA No.2056 ‘Dorothy’ would be fitted
with one.
There would be no need for a
reducing valve, even though the locomotive boiler runs at a higher
pressure than the crane’s boiler did. The steam gaskets will
need to in tip-top condition to handle the pressures – but the
pressure in the crane’s cylinders is determined by the load, not the
incoming steam pressure. (The boiler engine(s) don’t have
variable cut off.) The gaskets would naturally be overhauled, as
the steam crane’s cylinders, pistons and valve chests would be
overhauled anyway if we put the crane back into steam-powered service.
We’d upgrade the motion by fitting the crane with a mechanical
lubricator. The main challenge would be to allow for the
crane’s pivoting.
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PROJECT : Class 15F No.3052 ‘Avril’ Stoker
Motor Overhaul : (19 July)
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The methodological strip down
of the mechanical stoker’s two-cylinder engine for the Class 15F
No.3052 ‘Avril’ has been continuing, courtesy of our favourite
Stoker Man, Michael Thiel. The project has advanced to the
dismantling of the individual bit’s n’ pieces and including the
possibility of losing a few in the process.
Seriously though, when one is
looking at the overhaul of a reciprocating steam engine, all the parts
need to be cleaned up carefully before measuring up and making an
assessment of what needs to be done. Clearances can be so fine
that dirt or even layers of oxidation can upset measurements.
As befits the finer work
required, Michael ‘Stokes’ Thiel had moved his workstation, kit
n’ caboodle, indoors next to the machine shop with better and more
consistent lighting. It was more sociable for him too (Pic S01
below) – rather than being stuck out in ‘depot limbo’, hidden
out of sight in the dark, cool shadows cast between massive dozing
locomotives.
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S01 – The big machine shop bench is a
sociable, well lit place to work, in full view of
everyone and the workshop’s main walkway
passes right in front. Michael (Left) responds to the
flare up as the acetylene set is fired up.
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S02 – The two-throw crankshaft
assembly
has been temporarily assembled so the
clearances and wear can be checked.
Notice that just like a steam locomotive’s
main pistons, the crank throws are 90
degrees apart to avoid a dead spot with
both pistons at dead-center and no
resultant leverage on the rods.
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S03 – Polishing slight surface wear
off
from the crankshaft journals before refitting
the big ends and measuring. Notice
how the slipper type crossheads
make great crankshaft stands with their
semi-circular counterweight cut outs
Not many reciprocating engines come
with built in crankshaft stands!
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With the recent publicity
concerning a certain crankshaft, ‘Stokes’ Thiel was nervous and
defensive having me around with a camera. Such is the price of
fame. But I got a pic of the crankshaft measuring that is under
way. (Pic S02) Michael measured up the clearances twice,
once after an initial wipe down of the working components and once
again after the journals and eccentrics had been rubbed down with very
fine grade wet and dry emery paper. It might seem like an odd
and destructive procedure, as you wouldn’t want to apply too much
emery to a car’s crankshaft. (Especially if it’s case
hardened.) But remember that the parts for these locomotives are
no longer available off the shelf – so components don’t have to be
machined or manufactured to fit theoretical standard parts.
Obviously we try to conform to the original standards in terms of
dimensions, but more importantly they have to fit each other and the
frames or casings where-in they work. That’s why this is
called ‘fitting’ and the built-in ingenuity and craftsmanship
extends the lives of these increasingly rare parts – but it does
mean that internal parts from one locomotive may not be
interchangeable with another.
It’s an interesting remake of
history. Before Henry Ford pioneered the concept of mass
production for motor cars, many Edwardian and early 20th
century vehicles had to have parts lapped, cut and fitted by hand and
these parts were not interchangeable. Those long ago mechanics
had to be fabricators as well – real craftsmen.
But back to the depot … When
the crankshaft was first removed it was found to have normal slight
circumferential wear marks. The crankshaft journals were found
to have ovality of 0.15mm. With the big ends assembled with the
original shims, there is a clearance of about 1mm between the
crankshaft journal and the internal diameter of the bearing shell.
Yowch!) If this was a car engine with those clearances, it
would have destroyed the crankshaft and big-ends in short order.
On the stoker it results in knocking, which spalls the surface of the
journals, degrades the oil film and tends to hammer the journals oval,
which gradually makes the problem worse.
As stated, both the ball
bearing type crankshaft main bearings are to be replaced. The
replacement bearings and the oil seals have already been purchased –
safely wrapped in air-tight zip-lock bags and smeared with white
grease.
The big end bearings are
shimmed as standard and are currently fitted with a pair of 1.7mm
brass shims brass shims on either side. (Thus, the original caps
are shimmed at 3.4mm) Michael is preparing to make up his own
shims from brass stock and tighten up the big ends, without the hassle
of re-metalling and machining the bearing surfaces down again. (Pic
S04 below)
Pic S05 (Below) shows a picture
of a valve spindle as just withdrawn upon the initial dismantling.
The spindles were cleaned up today with very light machining on James
Thomson’s lathe and you can see the gleaming results in Pic S06
below. Everyone wanted to feel how smooth the finish was and
James Thomson was swatting us away because of our oily, acidic finger
prints. The valve ring grooves were re-cut and James is
preparing to cut new valve rings to suit. With the inherent
accuracy of James’ work, the final fit will probably be better than
when the Stoker first left the works. Michael will be cutting
and filing the slots of the eight fabricated cast-iron valve rings to
suit the measurements of each valve chest. (Four on each side.)
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S04 – A fistful of dollars, er, shims.
These are original Standard Stoker
Company style brass shims – shaped
to fit the big end cap as shown above.
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S05 – A valve spindle as just
withdrawn
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S06 – A pair of gleaming, newly
cleaned
and re-polished valve spindles ready for a
new set of four valve rings each, eight in
total – to be fabricated in-house of course.
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All the other parts were
cleaned and inspected, including the crosshead slides, the clevis
pins, the gudgeon pins and the pistons themselves. They are
booked for the next polishing exercise. In amongst all the
cleaning, the castellated gland nuts received some attention.
There are eight of these in two sets of four, all of brass, and all a
bit awkward to get at within the rod chamber. They are meant to
be removed with a C-Spanner, but it is all too easy to just whack away
at the radial slots with hammers, chisels and the like.
Naturally, over the years of service, and possibly attention from an
indifferent fitter or two, the castellations get mauled and rounded.
Eventually the c-spanner no longer works and the fitter has to resort
to more brutal methods, which messes the nuts up even more. This
was a monotonous job, as Michael had to hand file each one of the
slots. Luckily Michael was able to watch the antics of the 12AR
boiler tube gang, which kept him amused and occupied while stroking
the brass.
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S07 – These are the slipper type
crossheads
for the power pistons – notice the semi circular cut-out to
clear the counterweights. These are fitted with wedges.
The two clevis yokes are the crosshead couplings for the two
valve rods.
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S08 – The Fitter. That brassy
gear-like
device clamped in the vice is an end view
of a castellated gland washer. Michael had
eight of the fiddly things to dress with a file,
hence his wry expression in this pic.
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S09 – A choice assortment of newly
cleaned, dressed and machined conical
gland nuts for the piston rods. The
conical sealing faces are clearly seen
facing upwards. All the castellations have
been cleaned and cut a little deeper.
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A little more machining was
done, based on our experiences with the chevron seals that leaked so
badly on Class 15F No.3052 ‘Avril’s’ debut run. The glands
‘crush up’ and seal better against a tapered surface, rather than
a flat. The stoker piston rods use a split conical ‘olive’
to hold back the steam and these are ever more suitable for a tapered
conical sealing surface. Each one of the piston rod gland nuts,
after cleaning and dressing, was machined by James and the refurbished
results are visible in Pic S09 above.
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PROJECT – Class 12AR No.1535 ‘Susan’
Boiler Tubes
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Yeah…this project is finally
moving after months of us all seeing the seven boiler tubes lying
uselessly next to this old engine.
The delay was in the
availability of the boiler inspector and the fact that he had to make
some extra calculations to verify a potential issue that he found.
The lower section of the front tube plate is a bit thinned out and was
subject to extra scrunicity. It’s a vulnerable part of a steam
loco, as that’s where ash and char tend to collect. When the
deposits get damp via water ingress through the chimney, or form a
half hearted smokebox washout, the sulphur leaches into the water and
forms corrosive sulphuric acid. After a series of complicated
calculations and more measurements, the front tube plate of the 12AR
was deemed fit for another three year’s service after the boiler has
been tubed up and recertified.
Phew!
We’re keen to get this engine
running again, not just for her own sake, but because she’s
economical and yet a sure footed hauler. She has a good turn of
speed, in site of the small driving wheels. The engine is hand
fired, and is thus a great training platform. Our Class 12AR
No.1535 ‘Dorothy’ is the last Class 12AR in existence, let alone
still running and is an unusual sight. As strange as it seems,
overseas photographers do get a bit bored with the 25 and the 15’s,
whereas the 12AR is an unusual earlier class and always popular.
The boiler project was handled
by the Ackerman brothers today, each working on their own tasks.
Shaun Ackerman worked on preparing the boiler tubes and the tube
plates, while Patrick rounded up some tools and got busy fabricating
the copper ferrules for the tube ends. But firstly … Ackerman
Slightly Senior, hard at work in the steely sarcophagus of the
firebox. You could see the guys were psyching themselves up for
the job – collecting the tools and rigging up the 32 volt boiler
inspection lamp.
The 12AR has a short but tall
firebox and it’s always strange climbing in through the firebox door
and sitting on the grates, surrounded on all for sides and overhead by
solid steel plates decorated with the riveted heads of the boiler
stays. You can see through the grate to the ash pan below, and
in the center area – you can see right through the ash chute and
into the boiler trench. It’s dark and chilly inside the
firebox of a dead locomotive – in such contrast to the bright
inferno that is resident when the engine is running.
The first job of the day was
descaling. There’s nothing like a good stiff brushing and then
a tapping with a drift to knock the scale off. You can see the
newly cleaned area in Pic R01 below. The entire firebox is
covered with a thin, brittle black scale which comes off after the
surface is fractured and you can get behind it. Patrick and I
had much tactile satisfaction picking off the scale later in the day
while waiting our turn to work. When the boiler inspector comes,
the entire firebox has to be chipped out and cleaned to the bare
metal.
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R01 – At this angle you can clearly
see
the seven empty holes where the old
tubes have been removed. The light brown
colour is actually the lime scale on the
bottom surface of the boiler shell itself.
You can also see that it is the lowest two
rows of tubes that have been withdrawn.
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R02 – Cutting a slot in a copper
ferrule
to enable it to collapse and to be
punched out of the rear tube plate.
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R03 – A realistic sculpture of a tube
plate
is taking shape as the old copper ferrule
is tapped out. Notice that a copper mallet
is used – you don’t use a steel mallet on
a hard cold chisel in a confined space.
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With all the loose stuff taken
off, it was time to cut and punch out the old tube ferrules. The
2 ½ inch diameter copper rings that act as crush rings to seal the
ends of the tubes usually remain behind when the tubes are withdrawn.
Dr. Smudge Ackerman cut the rings down using the edge of a half
round file. (Pic R02 above) The job could have been done
quicker and cleaner with a hacksaw blade, but apart from the risk of
cutting into the tube plate, the resultant slot wouldn’t be wide
enough to allow the crushed-in copper ring to collapse. This was
uncomfortable work on these tubes in the lowest rows – as the
tapered file has to be held horizontal while the operator is squatting
on the haunches.
The tapping then began (Pic R03
above) and it could be heard from the front of the engine as the sound
passed through the boiler tubes. The ferrules were tapped
diagonally along the side of the newly-cut slots to force them to
twist, and one side of the slot to wrap and telescope over the other
half. They would then reduce in diameter and collapse.
Some of then stayed within the tube plate, and some of them got
punched right through into the boiler cavity and had to be fished out.
Plucking the ferrules out took care as those edges were sharp but the
clearances too fine to have clumsy thick-skinned protective work
gloves on. (Pic R04 below)
Patrick then climbed in to ask
some questions about the new ferrules he was making, and to compare a
sample with the originals. So there were three of us in the
firebox. Patrick tied the work light up to one of the fusible
plugs with a piece of wire that he had (Pic R05 below) – so Shaun
could use both hands. (I had no goggles and wouldn’t be able
to safely get close to hold the work lamp during the grinding.)
The yellow ear muffs came on to muffle the acoustic dingbats flying
around that steel echo chamber. (Pic R06 below) I turned
my hearing aids off – which then act like highly efficient custom
fitted ear muffs, and Patrick got his tail out of there. He’s
built like a rake and literally SLITHERS through the oval shaped
firing hole. Bit eerie to watch, actually….
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R04 – Gotcha! The last copper
ferrule
on the lower right comes loose. It fell
just behind the tube plate and could
be hooked out with wire and then fingers.
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R05 – A view through the firebox door
during a break in operations. Notice how tall
this firebox is. The lighter colour on the walls
show where the fire arch would normally be.
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R06 – the spark trail provides more
light
than the isolated 32V work lamp in this
non-flash exposure through the firebox door.
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The tube plate dressing
operation commenced with much noise and dramatic spark trails firing
against the right hand plating and skirling down through the ash pan
and visible from the outside. (Pic R06 above) The
objective was to strip the tube plate surfaces down to bare shiny
steel around the empty tube holes. Apart from the rust and dirt
that may remain after the initial descaling work, there may be
remnants of the original bead and welding remaining. When the
tubes will be fitted, the new ferrules are expanded into the holes,
and then the new tubes slipped in and expanded into the ferrules.
Then the ends of the tubes are ‘beaded’ – that is, bent through
180 and welded against the tube plate. The metal-to-metal
contact has to be almost perfect, and the material needs to be 100%
clean for a good, safe pressure and expansion proof weld. (You
can see some existing beading in Pic R09 below.)
The grinding went quickly (Pic
R07 below), even with frequent breaks to run a finger around the holes
to check for imperfections. Of course, it had to be allowed to
cool down a bit from all the grinding work. Luckily, the heavy
mass of the tube plate and tube metalwork acts as a good heat sink.
The power drill came into play next, fitted with a 2 ¼ inch grind
stone. (Pic R08 below) Shaun ran this carefully around the
inside surfaces of the holes to polish them up.
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R07 – The artist examines his work –
the clean dressed areas around the
seven empty tube holes. Looks a bit
like an old fashioned Siamese Port
Manifold set, doesn’t it?
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R08 – Polishing the inside mating
surfaces with a grind stone and a standard power drill.
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R09 – Shaun uses his fingers to check
for pits, dirt and imperfections. (It’s the
camera flash that makes it look bright.)
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PROJECT – 12AR Boiler Tube Ferrules ;
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While Ackerman Slightly Senior
was getting closely acquainted with a series of 7 holes in the steel
and carborundum scented air of the firebox, Ackerman Slightly Junior
was standing comfortably fully upright and tinkering with a 2 ½ inch
diameter copper pipe. His job would be to expand the pipe to 2
¾ inch outside diameter and to cut it cleanly into rings. The
individual rings needed to fit the width of the rube plate exactly as
well have having perfectly straight edges. These would be the
copper ferrules that would form a crush sealed joint between the tube
and the tube plate, and also to prevent water from getting in behind
the welded beading from the boiler’s water space.
Patrick’s copper ferrule
project started with a lot of necessary faffing around to get all the
tools together as they were to be found in various places. He
had to find his temper a bit too – it’s possible to waster over an
hour looking for tools and supplied in our sprawling depot. The
tube expanders are kept in their own lockable store at the Top Shed,
as are all the boiler tools and there was a delay in getting the keys.
Refractory bricks had to be found for the annealing, and the acetylene
torch set brought out. Even a bucket of cold water had to be
arranged.
Patrick was planning to use the
chuck of the nearby 7 ton Dean Smith lathe as a pipe vice, as it would
be vital to keep the copper pipe circular. However, the
lathe’s chuck key had gone missing. A new one had to be
fabricated before the job could continue.
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CF01 – A collection of tools neatly
laid
out. Note the sample ring. The vertical
objects at the back are the tube
expanders, and the tapered rods to
the right are the expander mandrels
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CF02 – The first round of annealing
with
an acetylene torch. Those are refractory
bricks from a dismantled fire arch
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CF03 – A smiling Patrick shows that
he’s finally having fun as he tightens up
the chuck of the 7 ton Dean Smith lath
as a pipe vice. Notice how the newly
annealed copper catches the flash light.
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The first stage of the job
proper would be to heat up the working end of the copper tube and then
plunge the red hot end into cold water. (Pic CF02 above)
This is the process of annealing the copper and actually softens up
the material to make it workable. The torch burns off the
impurities and oxidation from the surface too. The mass of the
pipe was small in relation to the water so it could be picked out
fairly quickly and placed into the chuck of the Dean Smith lathe (Pic
CF03 above)
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CF04 – The first of many rounds of
tightening. Here, the slanted rollers have screwed the
still visible top hat section right up against the copper
pipe. If this is withdrawn, and the tapered mandrel
pushed in further, you might get another few turns of travel.
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CF05 – The expanded pipe is in the
lathe
and the radial yoke, ready for the cutting
tool to be set up. The belled out, newly
expanded end can be clearly seen.
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CF06 – One ring to measure them all,
one ring to test them, one tool to expand
them all and in the boiler bind them.
(With steamy apologies to Tolkien.)
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Then the tube expander could be
applied. I never thought to get a close up picture of one of
these devices. They are that special combination of simple and
ingenious. Basically a tube expander comprises of a top hat
shaped cage, fitted with tapered rollers. The rollers can move
radially in and out. The cage is inserted into the pipe (or
boiler tube!) with the rollers slack, and then the tapered mandrel is
installed and gently tapped in. This pushes the rollers out and
firmly against the interior walls of the pipe. Because the taper
of the mandrel matches that of the rollers, their outer edges line up
parallel with each other and the pipe’s internal surfaces.
After a few taps to snug everything up, you then turn the mandrel.
It drives the three rollers, (by friction) which rotate the cage by
counter reaction. As the rollers are slightly tilted from the
longitudinal axis of the tool, they roll with a slight helical motion
and gradually screw the cage inwards. The tilted tapered rollers
also grip the mandrel, so it automatically moves inwards into the
cage. The rollers are automatically driven outwards by the
increasing diameter of the tapered mandrel. The radial outward
movement of the rollers is was stretches the tube – with an
unsettling rippling movement, rather like the rippling eyelids of
someone who is asleep and deep in REM sleep. (Dreaming.)
Pipe Expansion went as planned.
Unfortunately, if you stretch copper, it becomes work-hardened.
Patrick had to redo the annealing several times in between judiciously
adjusting the expanders (in three different sizes) and the depth of
the various tapered mandrels. It’s a fine balance between
getting the job down sometime today, and pushing it too far and
splitting the work piece.
The rings were to be cut in the
Top Shed’s lathe. This required that the tube be carefully
clamped in the chuck and the pipe yoke to prevent it from shifting
under tool pressure. Patrick had a surprise when he couldn’t
find a suitable tool and had to try and sharpen one for the job.
The second surprise came when he discovered that the top shop’s
pedestal-mounted grinder won’t start up and the power switch is
hanging out. Looks distinctly like a failure and somebody had
hopefully done some testing. Fortunately, the bench grinder
halfway along the shop, even with worn stones, at least powers up on
demand.
The cutting job didn’t go so
well with a tendency for the copper pipe to run out of true in the
lathe’s chuck. (it is soft material) Patrick persevered
though and not forgetting oil for the yoke and the cutting tool.
The job was finished with a hacksaw and then some careful filing.
The hacksaw, of course, was accurately guided by the deep cut all
around the pipe circumference. You can see the results on Pic
F06 above.
Meanwhile, back at the ranch,
or between the locomotives, Smudge has unfolded himself from smokebox
guts and started to prepare the boiler tubes. When we did the
15CA, the tubes had expanded ends and they were done with a dolly.
These new 12AR tubes are to be mechanically expanded and beaded – as
requirements are that replacement boiler tubes must be re-installed
with the same techniques as originally used in the boiler.
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BT01 – Cutting the standard length
of the tube down to fit the boiler.
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BT02 – Hand polishing a new tube end.
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BT03 – Very gently tapping in a copper
ferrule to be perfectly straight and flush.
A skew ferrule would distort under
expansion and end up grooved or
even cut by the tube plate.
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Shaun’s primary job was
cutting, de-scaling and polishing. These boiler tubes came in a
standard length of 6500mm and needed to be cut down to approx 6000mm.
When one measures boiler tubes, the tape must be passed through tubes
in each of the quadrants and the center as sometimes the tube plates
aren’t quite straight. Often they are bowed out slightly in
the middle, or may even be bowed inwards. The cut edges of the
tubes have to be 100% straight so the work, as clumsy as it looks with
a big grinder, was actually a precision operation. (Pic BT01
below) The tube was carefully marked around its circumference
with tape before marking with engineering chalk. There are no
spare tubes and thus no chances of fixing up a bad cut. There
have been stories of other steam people stretching tubes that are too
short or splicing tubes together – but we Reefsteamers work to a
higher standard than that!
The ends of the tubes were then
heated to an even medium orange before being allowed to cool
naturally. This anneals the ends, as well as burning off the
black protective coating applied by the manufacturer as well as any
impurities on the surfaces.
After the heating, came the
meticulous cleaning and polishing with fine graded strips of emery
cloth. The tube ends were cleaned inside and out. (Pic
BT02 above.)
Tube installation started with
the installation and expansion of the new copper ferrules in the
recently cleaned holes of the tube plate. Patrick did this with
care, after filing down the sharp-ish corners of the tube plate and
making doubly sure the mating surfaces were clean. The ferrules
also had to go in dead straight and be of suitable width for the
possibly variable width of the tube plate. The ferrules fitted
well enough and required a minimum of tapping to get them in. (Pic
BT03 above) This was done with frequent checks behind the copper
ring for protrusion and it was tapped down to be totally flush with
the firebox surface.
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BT04 – The tube expander has just been
withdrawn from the expanded copper ferrule.
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BT05 – With the camera optics poking
through the tube plate, here’s the void
within the boiler where the seven new
tubes will be installed. All that lime scale
is going to have to be washed out.
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BT06 – Gotcha! Lee and
Patrick’s fishing
expedition is a success as the pry bar
engages in the tube – now it remains to
wriggle it back, tilt the pry bar against the top
surface and feed the tube through the ferrule.
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During the day, with various
issues and delays, Patrick had only managed to make two new copper
rings for fitting as tube ferrules. (His third ring was the
sample) so it looked like only two tubes would be fitted today.
While Shaun was double checking his cleaning (by feel) and preparing
to slide the tube in through the front, the expander was in play.
It took quite a few rounds of expansion, adjusting and up-sizing to
get the copper ring to crush up evenly against the tube plate.
(BT04) And somehow you have to stop the tube itself from turning
so there’s relative movement between the expander and the tube and
so it can screw itself in. (The fellow at the smoke-box end does
the holding) By modern boiler standards, a large expander has to
be used as the ferrule goes around the OUTside diameter of the boiler
tube.
We were ready to try and put a
few new tubes in. They are literally fed in through the front
tube plate and because the holes are slightly wider than the tubes, it
can tilt downwards as it wriggles through the open space in the
boiler. (Pic BT05 above) The boys in the firebox have to
try and catch the end of the tube with a tool – a pry bar in our
case, and feed it into the appropriate hole on our side. My
trusty powerful MagLite torch can actually fir through the tube holes
so Patrick and I had the extra luxury of a decent spot light to try
and pick up the wavering, dipping end of the tube approaching us.
(Pic BT06 above.)
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BT07 – The tube expander‘s mandrel
being fed in to expand the rollers to the tube’s ID.
Note that the expander itself is held partially
extruded to provide clearance as it screws
itself in. Those long bony reverse jointed
fingers are a Patrick trademark and of great
use to him in model and real steam engines.
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BT08 – Two tubes home but only one has
been expanded within its ferrule. The gap
around the lower tube is clearly visible.
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BT09 – A locomotive sized ratchet
comes
into play as the tube properly fills up the
ferrule and the true expansion begins.
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It wasn’t too difficult to
make the catch although, due to the length and the weight of the tube,
it’s quite difficult for the fellow at the smokebox end to hold the
tube straight and still. The tubes came in just a tad loose.
There’s a problem visible in Pic BT06 (above) – you can clearly
see the scale that got picked up inside the tube as it dipped within
the boiler barrel. This was mainly raked out but the boiler will
need cleaning before re-commissioning and testing. During the
first expansion operation, Patrick aborted it due to newly deposited
dirt that he found between the tube and the copper ferrule.
The expansion operation went
well but was a drawn out affair with frequent adjustments of the
tapered awls and switching between two sizes of tube expander.
The unlatched drop grates were open too – so the risk of dropping
tools down through into the ash pan added to the interest of the
operation. (On the following day when Lee did some expansion
work, we couldn’t get No.1535 ‘Dorothy’s’ drop grates to latch
closed – so Lee blocked the open hole with a loose fire bar.)
The drop grates are actually functional, but somehow the
grate levers for the Class 12AR locomotive have gone missing.
While the levers from another locomotive mated with the pegs, the
angle of the ‘foreign’ lever was such that the handle bumped the
boiler backhead before the grate’s latches line up.
Initially one can turn the
expander by hand and then with an adjustable spanner. Then comes
the ratchet. (BT09 above) as the clearances close up and some
grunt needs to be put into the full expansion. But while doing
all this, the tube work piece must not be allowed to shift back and
forth within the tube plate. A protrusion between 8mm to 10mm
into the firebox is required to make the beading. Because it’s
a circular tube, it only contacts the tube plate on two points.
Thus, in spite of the weight, an un-expanded boiler tube shifts
surprisingly easily when it is suspended loosely between the 2 tube
plates. I almost pushed the bottom tube right through on the
following day and had to use the expander as a puller to get it out
again.
We ran out of time and only two
tubes could be expanded into the firebox end. It was decided to
leave the tools in the firebox and the team would have another go
tomorrow – Shaun in the smokebox again and little me handling the
tubes in the firebox. Unfortunately, one of the expanders went
astray and we couldn’t finish the job on Sunday either. Maybe
this week….
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PROJECT : Hunslet Taylor Shunter engine removal
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Like many jobs at the Depot,
the Hunslet Taylor gearbox repair project has become a big strip down
project. While the box of cogs were out, and a new final-drive
gear being fabricated for the jack shaft (At Surtees Engineering) ,
Reefsteamers took the opportunity to fix a long standing irritation
with the diesel’s 150HP type LX6 Gardner engine. It’s an old
fashioned 6 cylinder in line pushrod motor – with the cylinder block
cast in two blocks of three cylinders each. There’s a plate at
the end of the blocks, which closes in the cooling water jackets.
The front block’s plate was weeping and they are totally
inaccessible in between the two engine blocks when the engine is
assembled. Piss poor design – if you get the pun. It’s
only been a slight weep but it has ensured that it’s uneconomical to
use antifreeze. (There’s a lot of rust visible within the
water passages.) And all it would take would be for someone
unfamiliar with the fault to start the engine without checking the
water first, innocently do some shunting and overheat the engine.
The locomotive does not have a temperature gauge. This
engine’s cooling system is of the old thermo-siphon type and
doesn’t have a water pump. A dangerous characteristic of the
thermo siphon system is that if the water level drops below the bottom
of the top radiator hose’s entry into radiator’s header tank, the
water circulation totally ceases. This large engine has
tolerance of less than a 2 inch drop in the water lever whereas a road
vehicles engine would continue to run.
The oil pump isn’t working
properly either. Dropping the oil pan to reach the pump turned
out to be a major awkward job – testing patience to the limit.
It’s been decided to bite the bullet and just take the entire engine
out. There have been some grumbles about the continued stripping
and thus the extended unavailability of this shunting engine.
But it’s uneconomical to do just half a job. For the cost of a
bit of extra downtime now we’ll have a solid reliable diesel shunter
locomotive for years to come. Furthermore, this engine has never
really been restored – so it needs a lot of work to get it to
standard. And to be honest, it hasn’t really been all that
well looked after – often being parked out doors in the weather and
the maintenance has been reactive instead of pro-active. We plan
to tidy up the cab, replace the missing windows and to repaint the
engine in Hunslet green, with a black under carriage and the buffer
beams, rods and counterweights in red. Should look great when
it’s done!
But firstly, some photos of
what’s been done for the gearbox.
The gearbox case has been
externally cleaned and the sections loosely stacked (Pic G01 below)
but the interior needs to be thoroughly cleaned out as there are still
metal filings and shavings in there All the exterior bearing
bosses have been machined to 6mm wider than standard to be able to
accept 3mm thick spacer rings. (Pic G02 below)
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G01 – Gearbox casing waiting on a
trolley. The hole at the right top is for the pilot
shaft right behind the drive couplings.
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G02 – One of the eight new
oversized spacers – here next to
the RHS transfer shaft bearings.
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G03 – A worn out shim that was
previously fitted in a futile attempt to
stop the bearing races from turning..
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There is evidence that the
fixed outer races of the bearings were turning within the case,
especially on the bearings with contamination and rust damage.
As the gearbox casing material
isn’t designed to withstand friction – it created an extra wear
point between the bearings and the frame as well as within the
bearings themselves. It was the resulting misalignment in the
shafts, which naturally tend to separate under geared load, which was
causing abnormal gear wear and rough operation.
It looks as if the gearbox has
been removed and stripped before. The previous mechanics had
attempted to resolve the bearing carrier wear problem by putting in
thin brass strips as shims between the outer races and the frame.
This is bad practice as it puts uneven stress on the outer bearing
race and the shims eventually grind down with the relevant movement
anyway. You can see the tattered remains of one of the spacer
shims in Pic G03. (Above.).
All the bearings are to be
replaced with brand new ones of the original, slightly more expensive,
imperial sized bearings. There was originally a debate about
refitting the gearbox with modern metric sized bearings – but the
cost of the outer spacers, and then re-machining the shafts, outweighs
the advantages.
The main shaft has been
serviced and cleaned up. The worn splines at the pilot end had
been re-chromed and then re-machined. (Pic G04 below) Two
of the stop nuts had been remade from scratch, using an intact
existing one as a pattern. You can see them at either end of the
main shaft in pic G04 and a contrasting pair of loose nuts in Pic G05.
(Below) These nuts are deeply grooved to accept a large
spring clip.
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G04 – The main shaft with the entire
section to the right of the dark stop-
collar re-chromed and re-machined.
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G05 – An original and a newly
fabricated stop nut side-by-side.
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G06 – The cylinder block end cover
that was leaking. (It’s the long oval plate seen just
in front of the piston that is being held clear.
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The diesel engine itself has
turned out to a bit of a nightmare project for Andrew and Aiden who
both would like to get involved in a locomotive boiler removal and
refit as a light diversion.. For such an old fashioned engine,
which are usually simpler and more accessible, it has a lot of
accessibility problems and these fellows have spent many uncomfortable
hours sitting on their haunches on the narrow running boards. (Pic
G07 below) There isn’t enough room to sit on the running
boards and put your legs down by the side of the engine, and if you
sit cross legged, you can’t get close enough.
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G07 – A precarious and uncomfortable
ledge on which to work. Aiden spent
most of two Saturdays with his tail
dangling over empty space.
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G08 – A dirty cylinder after having
the
outside quickly wiped. Note the black sludge to the
right of the rocker shaft bearings. Note also that the
machined mating surface is correctly supported on wooden
blocks.
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G09 – Cylinder head bath time.
Not a remarkable pic until you remember this is
a cast iron cylinder head, with the valves still fitted and of
the heavy duty construction for a diesel engine too.
That’s quite a weight to have to keep shifting and topping
around.
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The engine’s bolts are of
strange sizes too. Some old spanners had to be filed thin, and
jaw sizes altered to suit. The photographs were hard to get in
the confined space and the fact I was shooting into the work light.
And Aiden was looking a bit grumpy... But I did get some
pictures of the later stages of the operation.
Today (12 July) while Andrew
and Aiden were tackling the removal of the oil pan to get to the
suspect oil pump, a brand new Reefsteamers member, Lucas Dreyer was
tasked with cleaning the removed parts. He did the job in four
stages. First came the crude oil and dirt wipe. (Pic G08
above) The rocker chamber and the pushrod risers were found to
be filthy. In fact, there was no bare, clean cast iron visible.
The extent of the dirt is one reason why Andrew wants to drop the oil
pan and also to inspect the oil pickup strainer and blow out all the
possibly half-clogged oil galleries. You can’t run an engine
like this as a blocked oil gallery will seize a bearing.
After a wipe down, both the
cylinder block and the head were brushed with paraffin to loosen and
shift the oily deposits. Then they were treated to a WAP high
pressure steam wash. Lucas uses these machines in his place of
employment, so he’s been added to the limited list of Reefsteamers
permitted to use the WAP machine. After the WAP steam lance
treatment, came the wipe down and dry off. The oil passages
still need cleaning but at least the castings can be inspected.
The inlet and exhaust valves are to be removed as new valve stem
guides and oil seals are to be fitted.
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G10 – A upwards shot into the belly of
the beast. Andrew is loosening the
sump pan’s flange bolts right under the
crankshaft pulley – the radiator (with
deeply cowled fan) is just to the right.
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G11 – A whole lotta work involved in
getting this little oil pump out from within
the sump. It was found to have moderate
wear and overly sharp gear teeth.
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G12 – An unusual feature for a 1952
year diesel shunter engine – helical-cut
oil pump gears. Notice that the idle
gear actually runs on a bronze bushing.
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The sump oil pan was a bugger
to drop with very stiff and awkwardly sized bolts. In fact, only
the very front and rear bolts (Pic G10 above) were directly accessible
from underneath, the most natural location for working on a jacked up
engine. The rest of the bolts had to be undone from the sides
with modified spanners, applications of vice grips and the like.
The sump pan would only go down
a few inches and the removal of the oil pump as actually a side-ways
caesarian operation through the small gap. The cute lil’ green
critter is rapidly becoming a bit of a monster.
The oil pump came out in the
late afternoon and was immediately dismantled. (Pic G11 above)
Wear in the pump was found to be moderate and the gear teeth have worn
sharp. This means a lower volumetric displacement. The
gear teeth were found to be of helical cut. It reduces the
contact pressure between the teeth and makes for a quieter running
device – but it’s an unusual feature in a diesel engine of this
vintage.
It seems odd that an oil pump,
that runs in oil, would ever wear out but one needs to remember that
the oil that is pumped is unfiltered. Only the gauze pick up
screen protects the pump itself. (The oil filter is always after
the pump in the lubrication circuit.)
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PROJECT : Sandstone Coach Repairs
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C00 – The Sandstone Coaches being
shunted out of storage in Ficksburg
– Saturday, 7 October 2007. These are the coaches in
the colour scheme
in we received them. Note the old fashioned riveted bar
framed bogie
with the traverse elliptical leaf spring as primary
suspension.
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The pressure is definitely on
for the coaching team and they are creaking a bit as they take some
strain. And I mean that literally – after seeing ‘The Sarge’
limping after wrestling with mounting bolts under coach seats.
Many of our original 2nd Class main line sleepers are out
of action as they are presently being converted into luxury coaches
with on-suite bathrooms for the Sitemela Consortium – a new railway
touring company. So we’re a tad short on coaches. And
Lawrence ‘Sputnik’ Posniak, of the South African Railway and Steam
Museum (SANRASM) has worked his usual magic and has booked over 600
passengers for our next trip when the new season starts in two weeks.
On day trips, we would
typically use a sleeper compartment as a private compartment to seat
up to six adults although eight ‘smalls’ can fit in and the kids
can recline on the upper bunk. But because these compartments
are accessed by a corridor, there can be no seating right opposite.
So in the space where a sleeper compartment seats six people – a day
sitter coach (basically, a bus) can seat ten. Because we are
limited in the number of vehicles we are allowed to haul, and one of
them has to be a water tanker and the power car (with crew
accommodation) the seating capacity on a trip is limited. Take
away one or two vehicle ‘slots’ to allow for the kitchen, lounge
or bar car and you’re left with about 8 coaches that can earn ticket
revenue.
It is high time that the four
privately owned coaches that were transferred from Sandstone Estates (Pic
C00 above) to earn their rail-space. Of particular interest in
this exercise are the two ex-Sandstone 3rd class day
sitters – each with a maximum seating capacity of 96 people.
For safety and insurance purposes, we can ‘only’ take 76 seated
people in each coach, but that’s almost twice as many as a sleeper
coach.
These coaches are basically
running okay with decent (rather vintage) bogies and brakes.
Before they are put into main line service, they will obviously have
to be inspected and running faults put right – but all four coaches
behaved well on their last 460km trip from Ficksburg. They
looked decent upon arrival too, with fresh solid red paint jobs and
recently painted undercarriages. However, the interiors are a
little ratty from many conversions, the interior floors have
delaminated and some of the seats are in poor shape.
Perhaps the most time consuming
problem is that the toilets had been blanked off with sheet metal over
the doors – and we had some unpleasant (but non-organic) surprises
when opening up the toilet compartments once more. It wasn’t
really an optional job though, as 150 plus passengers without toilets
could be nasty. One of the gangways had been blocked off too –
for service at the end of the train – instead of the proper
double-leaf vestibule doors and the external man-gate as used by SAR.
The Reefsteamers started this
project last week after the coaches had been shunted out into the open
after the elliptical roofs had been re-painted. The original
roofs were painted silver. They have since been repainted dark
grey with weatherproof polyurethane paint. (Pic C01 below)
Victor did the painting – he
started as a casual labourer but due to his reliability and skill, he
has since become a permanent employee. He also masked out the
sides and applied the French grey strip that runs alongside the
windows. The original paint job was solid gulf red all over.
As the paint was in good condition, it just needed cleaning before
applying the masking. After the painting, the high mounted
marker lights, the bogies and the center lamp shields would be the
only end feature that would easily distinguish the ex Sandstone
Coaches.
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C01 – A tale of two roofs. A
picture taken
on a cloudy day, you can see the original
silver roof on the right and the robust
new waterproof paint on the left side.
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C02 – A short lived train-spotting
feature – the ex-Sandstone coaches all had roof mounted tail
markers. These are being removed to standardize the
coaches – and they don’t meet railways standards anyway.
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C03 – A nice touch – the classic
union carriage and Wagon Co. builder’s logo has been
highlighted in black. This particular coach was built in
Nigel in 1971.
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