|
BACK TO
REEFSTEAMERS INDEX PAGE
|

|
Reefsteamers Depot News
Report
- wEEKEND 10-11 MAY 2008-
|
Introduction :
|
|
We’ve had Reefsteamers
beavering away at the Germiston Steam Locomotive Depot all week, as
well as a large crew of casual labourers working on the yard
clearing project and providing environmentally friendly propulsive
power for the tool trolley. Fred ‘Sparky’ Sewell got to continue
on his finishing-up work on the beautiful new Club House, which has
worked out very well. It’s hard to believe it was once a
derelict ablution block. Our main planned project for this
Saturday Depot Day was originally to be a combination of axle
bearing work and re-installing the overhauled stoker motor on the
Sandstone Estates GMAM Garrett No.4079 ‘Lyndie Lou.’
Best laid plans … And all
that.
Our little green critter of a
diesel shunter suddenly ended up on the sick list with a damaged
jack-shaft drive gear. It’s been an awkward time to have the
shop shunter out of action. We have been making a lot of
rolling stock movements, including revenue earning work for the
Shongololo Express. The Booth steam crane No.96 ‘Shosholoza
also had to be moved to help clear scrap metal and to be used to
finally get our enormous 7 ton Dean Smith lathe into its proper
position in the main workshop. Class 15CA No.2056
‘Dorothy’ has been in steam all week – having the fires nearly
completely dumped every night, a small bank made up and a fresh fire
lit-up from the embers under a still-warm boiler in the morning to
raise steam once again. (We can’t ask volunteers to do loco
minding during the week as they have to come in from work and then
go to work the next day – with a night of no sleep or just cat
naps.)
The 150HP Hunslet Shunter
uses a single speed gearbox with manually selected forward and
reverse. It also incorporates the final drive gear train,
which consists of 90 degree bevel gears and a final reduction set to
drive the counterweighted jackshaft that turn the two axles via
simple external coupling rods. The gearbox is prone to
moisture contamination within the gearbox oil, as it is poorly
vented. The fact that the diesel is usually stored outside is
another factor – we’ll be storing it under cover from now on.
(Now that the depot has been sorted out, we have the covered track
space.) It appears that as the bearings were wearing on the
jack shaft, the gears physically moved further apart, destroying the
mutual relationship of the involuted curve geometry and driving only
on the gear crests. One of the gears stripped and the little
green critter has lost its drive. He was shunted into the
number 4 road of the workshop, occupying the tracks recently vacated
by Class 15F No.2914 ‘Spikkels’ and worked on immediately.
Within the depot workshop, we
had three work teams working in two adjacent tracks. Michael
Thiel worked on and contorted himself around the GMAM stoker motor,
Dawie Viljoen and Shaun Ackerman focused on the Bissel Axle
replacement therapy while Patrick Ackerman and Kenny Allen worked on
the shunter. Andrew King was supervising the jacking and
blocking of the tender of Class 15F No.3052 ‘Avril’ as we
prepare for bogie overhaul and undercarriage cleaning.
An exceptionally busy day
with much action – so let’s read on about what was happening…
|
PROJECT : Disengaging the Hunslet Taylor
gearbox :
|
|
|

|
|
FPA – A timeless, busy railway
workshop scene. Working on the axle is Andrew King (Left),Shaun
Ackerman (Center) and Dawie Viljoen (Right) Sitting
next to the Hunslet Diesel is Kenny Allen, while standing
underneath is Patrick Ackerman. Michael Thiel is out
of view within the stoker engine’s recess behind the GMAM
cab to the right.
Edward, a new employee, is working on No.3052 Avril in the
next track.
|
The little green critter
eventually gave birth to a red critter that held on tightly to mamma
with every bolt, flange and shaft at its disposal! Read on how
Drs Ackerman and Allen performed the reluctant caesarian.
Preparing the locomotive for
gearbox removal was crude work, as befits the technology of a 1952
model, but the work wasn’t a mental brain buster. But the
gearbox itself is a surprisingly bulky unit that takes up most of
the under floor space of the cab. The longitudinal pilot shaft
and the counter shaft lie in vertical orientation to each other, and
the transverse jack drive shaft, with the characteristic external
counterweights, lies below the center line. Thus, there’s 3
‘layers’ of shafts in the housing. The final drive after
the bevel gear is through triple gears, including the large
fixed-ratio reduction gearing required to amplify the torque.
Our boys ended up trying to remove a tall, long heavy unit that
wouldn’t move backwards and wouldn’t move down. And then,
on the following day, it couldn’t be traversed through the wheel
drop pit without some extensive jacking operations. It made
the dropping and traversing the Bissel Trucks on the GMAM Garrett
No.4079 ‘Lyndie Lou’ look fairly simple by comparison.
In the preparatory
obstetrics, the center section of the shunter’s wooden cab floor
had already been lifted, consisting of several well-weathered 1 inch
thick hardwood planks. (Pic A01 below) Actually, those
floor boards came in very useful later on as narrow hard-wood
packing shims under the buffer beams! The gearbox has two
plain flat rectangular inspection plates which were unbolted and
removed to reveal the interior for a somewhat gloomy inspection by
the Chief Engineer, Andrew ‘Noddy’ King. The gear teeth
and those of the bevel gear set were found to be in reasonable
condition. This is a constant mesh gearbox – forward and
reverse being engaged by dog clutches, which displayed moderate wear
as can be expected after 56 years of operation. Being a
constant mesh gearbox, the main gear wheels in the drive-line are
not physically shifted longitudinally in and out of mesh, thus
little wear is evident. (This is actually a more advanced
system than the reverse gear of many modern road cars, which still
use an intermediate gear that is actually slid in and out of mesh.)
|

|

|

|
|
A01 – The general layout of the
gearbox just under the cab floor. That’s the
disconnected and chained up drive coupling to the right.
The bevel gear can be clearly seen. Notice the rusty
brown of the water contaminated oil.
|
A02 – The jack shaft bearing of a
coupling rod in storage on a convenient walkway.
Notice that this diesel’s coupling rod is grease
lubricated in classic steam loco style.
|
A03 – Under the belly of the beast,
Kenny Allen gets to work with a pair of spanners to get one
of the several dozen mounting bolts off. Notice that
the drop
pit’s jack hasn’t been extended yet.
|
The three through-bolts for
the pilot drive coupling were undone and the engine half of the
coupling slightly retracted. The gearbox is connected to the
torque converter via a short, shallow-angled universal-jointed
shaft, so it was easy to ‘bend’ the shaft and swing the engine
half of the pilot coupling upwards and away from its mate. The
loose drive shaft was chained to the throttle cross-rod that spans
the cab between the two throttle levers. (This locomotive’s
cab is ‘dual control’, the throttle and gear lever controls
being duplicated on both sides. As the brake wheel is on the
left, we usually run this engine ‘left hand drive’ – opposite
to that of our steamers.) You can see the light weight chain
to the middle-right of Pic A01. (Above)
The first wrinkle in the
operation was that the pairs of clamping bolts for the dual gear
levers were not accessible from within the cab. The gearbox
would have to be dropped with those long red levers still attached
and they would eventually only be uncoupled and removed at about 4pm
the following day.
The coupling rods were then
removed. This being a ‘little’ two axle locomotive, this
was a relatively simple operation and the main rods were removed
with the jackshaft sections still attached. (Pic A02 above)
This is going to be a good opportunity to check out those bearings
and try to knock out a few more clanks. The walkways alongside
the engine hood provided very convenient shelving for those coupling
rods. Patrick and Kenny then started removing the gearbox
bolts themselves, being careful to leave enough loose bolts in place
to hold the weight of the gearbox. (Which is just a bit much
for the hard hats to handle.) Because the gearbox on this
locomotive also incorporates the final drive, it must handle the
torque reaction and the counter-thrust imposed by the coupling rod
sets – hence its robust design. The design uses a series of
bolts located in 3 planes to transmit the drive forces and
distribute them into the frames.
All the gearbox fasteners
were hexagon bolts with equally hexagonal nuts – no captive bolts
were used. No rivets were used either, a major blessing in
that confined space. But the double ended fasteners all
naturally required the use of two spanners, with some creative use
of assorted pipes, gwala bars and wood blocks to wedge spanners into
place. The spokes of the primary drive wheels (rear axle)
provided many convenient blocking points. Patrick Ackerman
quickly realised that the diagonal bracing for the cab steps would
get in the way, so he hauled himself out the inspection pit and got
to work ‘de-bracing’ the steps while Kenny Allen continued to
work on the intermediate bolts. (Pic A03 above)
Kenny Allen isn’t a
frequent fixture at the Germiston Depot, as he is away studying
Mechanical Engineering in Stellenbosch. However, he is a
committed, popular young Reefsteamer and is willing to use some of
his usually rare holiday time to spend a day getting greasy with us
at the Depot. He is competent both with his hands and on the
footplate – and he is always a welcome sight amongst the regulars.
Kenny … it’s appreciated.
Now that I’ve embarrassed
Kenny, (Safely at the opposite end of the country!) back to the
commentary. Eventually both the youngsters got the step
brackets off. Only one end of those braces were bolted, the
other end welded. So they had to be ground off and will need
to be re-welded to the step backing plates upon re-assembly.
With no braces, the double steps would swing inwards if one
attempted to mount them – a uncomfortable feeling when the steps
in question are dangling over an open wheel dropping pit. The
long defunct sanding gear boxes and the drop-pipes were removed as
well. A further issue arose when it was found that the upper
bolts on the leading wing flange are obstructed by the axle boxes
behind the wheels. There was a bolt behind the leaf springs
too and it could not be reached.
This job was about to get a
lot more interesting….
|

|

|

|
|
A04 – Behind the drive rods
there’s a
wheel. Behind the wheel there’s a
bolt. Behind the bolt there is an
engineer – who is a bit behind on
practical ergonomics.
|
A05 – Jacking the axle. You
can
see that the axle box keep plates
have already been removed.
|
A06 – The chore of opening up the
drop pits.
|
The Chief Engineer was called
in for advice and it got crowded under those frames with four of us
under there. The decision was made to drop the rear axle to be
able to access and remove those bolts. Remember that the
coupling rods had already been removed so the job was actually
simple. The wheel drop pit’s jack was pressurized and used
to lift up the axle while the simple 2-bolt axle box keep plates
were removed. (Pic A05 above) The axle had to be lifted
to compress the leaf springs, get the weight off the axle boxes and
to disengage the wheels from the pit’s bridge rails. The
next step was to open up the wheel drop pits and to uncouple the two
bridge rails. (Pic A06 above) Opening the wheel drop pit
is never too easy a task as the expanded mesh covers gets wedged in
their channels over time, with all the tromping and walking going on
overhead.
With a minimum of swearing
and no mangled fingers, the cover was removed and the now-unloaded
bridge rails moved aside in a classic two handed wriggle. The
rear wheels dropped cleanly (Pic A07 below) and the last awkward
gearbox mounting bolts were able to be removed – with the
assistance of 2 feet of boiler tube as a spanner extension.
I’ve often said that we Reefsteamers don’t miss much. If
Reefsteamers were pork butchers, we’d use the entire pig except
the squeal. And in this case, we didn’t miss the opportunity
to lubricate the axle horn guides. (Pic A08 below.)
Another ‘pig squeal’ job was the scraping and cleaning of the
axle box keep plates before jacking the axle back in and refitting
the keep plates. (Pic A09 below) They presented little
trouble, each only being held on with two bolts. Jacking the
axle and guiding the freely pivoting gearboxes back into the horns
was, as always, a three man job.
|

|

|

|
|
A07 – A lowered wheel clearly
shows the classic brass axle
box as it clears the axle horns.
|
A08 – A set of axle horns. The
uppermost visible hole in the red gearbox housing flange is
the lower of two gearbox bolts that tangled with the axle
box and spring area.
|
A09 – An awkwardly positioned
Patrick (Because of the pit jack) replacing the
newly cleaned axle box keep plate.
|
With this done and the two
axle boxes all buttoned up once more, the wheel drop pit’s bridge
rails could be grunted back into place and the rather battered
fishplates re-bolted. The pit jack could now be retracted, and
freed up ready to block up the gearbox’s sump. This meant
that the entire locomotive had to be moved forward – so the brakes
were screwed back and a pair of pinch bars used to line the gearbox
up with the pit jack. (The rear axle crosses the frames in
front of the gearbox – remember this point as it comes up later!)
Now a wood block could be
fitted between the sludge sump and the oil pan, and the gearbox
carefully nudged upwards to take the weight off the last few bolts
holding it in place. Because the pit jack has extra brackets
and braces on the working head, which fouled with the deep sludge
sump, the jack’s head had to be cut down to a simple U-shape to
complete the job. (Pic A10 below) So the acetylene torch
was brought out to modify the jack before the gearbox could be
propped. Reefsteamers often modify their own tools to suit the
purpose.
The propping had to be done
very carefully, as if the pit jack was allowed to be over-extended,
you’d end up lifting the weight of the entire rear half of the
locomotive with the frames literally hanging on the gearbox,
possibly bending or shearing those bolts, and fracturing the
castings. The gearbox was propped and the bolts removed.
However, the front wing flanges of the gearbox got hung up on the
protruding axle boxes. (Pic A11 below) There was
insufficient movement to move the gearbox backwards to clear the
axle boxes – so the Hunslet mechanics were a bit stuck.
|

|

|

|
|
A10 – Patrick cuts down the extra
wing braces on the pit jack before it can be
used on the flat faced sump. That’s
the RHS brake rod in the foreground.
|
A11 - Snag point. Here’s the
protruding wing flange that was just wide enough to hang up
on the protruding axle box. (Lower right)
|
A12 – if you can’t tilt the
gearbox, you
can certainly tilt the locomotive!
|
As it would be dangerous to
tilt the gearbox on the stand, it was decided to tilt the locomotive
relative to the gearbox. At the same time, the jacking would
be necessary, anyway, to suspend the locomotive once more as the
bridge rails would need to be removed again. (To allow the
protruding counterweights and drive pins of the jack shaft to pass
through.) A pair of small ‘Buda’ bottle jacks were
extended under the rear buffer beam. (Pic A12 above) These
‘small’ jacks have a 25 ton capacity, which, in steam locomotive
terms, is as light as a ballerina’s lunchbox. The upward
movement would have the effect of swinging those obstructed flanges
back from the axle boxes and downwards. Unfortunately, there
was insufficient clearance at the back of the frames to allow the
front end of the gearbox to clear.
After some head scratching
consultation with the Chief Engineer, who lost a few more of his
increasingly sparse grey hair in the process, it was decided to
literally cut down the protruding wing flanges by a few millimeters
to clear the axle box. It’s rather a drastic solution but as
the mounting arrangements are massively over-engineered, the loss of
metal would be insignificant. Soon, the workshop resounded to
the sound of a nervous Patrick cutting down those flanges with a
small disked angle grinder and trying frantically not to accidently
cut weakening grooves into the frames.
|

|

|

|
|
A13 – Investigating the problem.
That’s Patrick Ackerman yet again repositioning
an enclosed, caged 32V inspection
lamp that was a pure nuisance with local glare and the wire
getting in the way.
|
A14 – The boy stood on the burning
deck,
his pockets full of crackers.
The sparks flew up his trouser leg,
And promptly blew off his …..
|
A15 – A rear view of the bulky red
abortion being lowered out from under Mamma. Notice
how the sump fits neatly around the jack.
|
In fact, he left a thin web
of metal on the outer flanks and chiseled the pieces off. I
couldn’t get a decent shot of the angle grinder work due to the
close quarters. But check out how the spark trails flew up
past the gearbox, through the floorboards and into the cab in Pic
A14. (Above)
With the wing flanges
slightly cut down and some very judicious wriggling, the massive,
clumsy gearbox housing could be removed. It was gently lowered
on the jack, the flat surface of the oil pan and neatly protruding
sludge sump neatly interlocking with the jacking block and thus
helping stability. You can see a neat end view in Pic A15
(above) As the box was lowered on the jack, the drive coupling
and the rear axle tried to occupy the same space (Pic A16 below)
– which is now why you know I told you to note the axle
position. . It was at this point the work team packed it
in for the day and got busy tidying up. The day’s
Magaliesburg train would be coming in at about 6pm and the engine
(Class 15CA) would need to be coaled up and serviced. Andrew,
meanwhile, could investigate the strategic situation and what tools
would be required to remove that obstructive main shaft.
|

|

|

|
|
A16 – The red pilot coupling hangs
up on
the rear axle. This was the last snag that ended the
work for the day – time to go
and prepare for the incoming train.
|
A17 – The removed main shaft and the
pilot coupling half. Andrew is standing awkwardly
akimbo as he cleans off the rear gear before slipping it
over the splines for safe keeping.
|
A18 – The gearbox bottoms out on the
pit jack and is blocked from traversing. We had
already starting jacking up the locomotive at this point –
the wheel is already airbourne.
|
The project continued at a
more relaxed pace on the following day (Sunday) with the removal of
that main shaft and the blocked coupling half. (Pic A17 above)
Fortunately there was enough room to pull the shaft forward between
the empty frames, over the axle and under the drive shaft area.
With the main shaft and the pilot coupling gone, the gearbox could
be lowered even more. But ‘even more’ wasn’t enough as
the wheel drop pit jack then dismally bottomed out. (Pic A18
above) Great. The little green critter was turning out
to be a big monster.
One of the old sack trolleys
was pressed into service and a choice assortment of wooden blocks
were fetched. One advantage of a recently cleaned workshop is
that one at least knows where the tools are! Patrick and Lee
jacked up the engine – first with a large 50 ton ‘Buda’ jack
under the front coupler base and the rear end on blocks, in a tripod
arrangement. Whenever we Reefsteamers jack a railed vehicle,
we constantly mix and match the wood blocks to try and get their top
end as close to the buffer beam or frame as possible – so should
the jack slip or collapse, there’s a minimal distance for the load
to fall. It slows the job down, switching the wooden blocks in
and out … but safety first. You can seriously hurt yourself
with all this weighty equipment!
|

|

|

|
|
A19 – Jacking up a locomotive, even
a
‘small one’ like this, is a great tummy toner! Us
Reefsteamers don’t need Virgin Gym subscriptions – we
get our regular
workouts and have fun doing it too.
|
A20 – The twin gearlevers are now
accessible under the jacked up engine.
The edge of the wheel channel at the
bottom of the picture shows the ground level.
|
A21 – The gearlever handle clamp has
two side-by-side bolts and these were easy to remove.
That grey gunk is track dirt while the white stuff is steam
locomotive ash.
|
With the locomotive’s front
end supported on two sets of blocks, the rear end was then jacked up
using the coupler base. We ended up with both the jack and the
supporting blocks based on cross beams spanning the inspection pit.
It meant a heavier load on the jack (and the operator) but
eliminated the need to coordinate two jacks for stability.
This method maintains a tripodal arrangement that is automatically
self leveling – like a three legged milkmaid’s stool. Lee
and Patrick took it in turns but Lee ‘Flash’ Gates eventually
took over the operation. (Pic A19 above) Poor Patrick
had tacked a lunchtime Cornish Pasty, which tackled him right back.
With all the calisthenics of operating a jack, he quickly felt
nauseous, working slower and slower, visibly deteriorating until the
pie finally defeated him and he disappeared discretely to the
toilets to blow his chunks.
Patrick came back, black of
eyes and white of face while we were disconnecting the dual gear
lever rods. The height that we’d gained in jacking the
locomotive relative to the bottomed out jack meant that the gear
levers, clearly visible in Pic A20 (above) could now be removed.
This was an in-and-out job, as it’s really not a good idea to work
under a suspended lump like this, as stable as it may seem.
Fortunately the double-bolted clamps would be easy to remove.
Well, with the protruding
gearlevers removed, and the locomotive perched on wooden blocks, the
gearbox was now free to move out from under the frames and from
under the rear wheels. The I-Beam wheel channel and the bridge
rails were moved off to one side to clear the entire wheel pit to
the right of the locomotive. Meanwhile, the dismembered
gearbox was ratchet-strapped to the base of the wheel pit’s jack
for safety. (Pic A22 below) It wouldn’t do to have
this lump rolling off the jack in transit. Traversing the
gearbox went without incident. Patrick just sat miserably on a
drum, his sensitivity to cold not being helped by a thin overall,
and his stomach doing it’s best to scramble up his esophagus.
The LPG gas powered Hyster
forklift was fired up and brought up to the wheel pit. Two
blocks of wood were placed to provide an extra few inches of surface
for the front wheels to extend the reach as far as possible. (Pic
A23 below) Two 6 ton capacity lifting straps were used to
hoist the load out of the pit, and it the lifting went smoothly in
two increments. The load hardly swung and we didn’t even
leave any red paint on the pit wall.
|

|

|

|
|
A22 – All strapped down and
somewhere
to go. The gearbox has been rolled out sideways ready
for lifting. You can see the ratchet strap in between
the two inspection apertures in the top frame.
|
A23 – Just-one-more-inch. The
blocks are actually there to extend the wheel path.
|
A24 – The camera flash fired and
closed the iris for this shot – but you can see how the
gearbox lifted well at almost the full reach of the forklift
tines.
|
Andrew then backed up the gas
forklift, Patrick moving out of the way, looking even sicker with
the LPG carbon-monoxide fumes. I assumed he was instinctively
crawling off to find somewhere quiet and private to die … until I
got a whiff of those fumes myself. The forklift was backed all
the way up the workshop area. It was done in little increments
and with gentle brake applications, as not to cause the heavy load
to start penduluming in suspension. (Pic A25) the load was
parked at the storeroom end of the workshop, which has recently been
cleared of junk and spares in the recent cleanup. The only
obstacle encountered was a ½ ton inglenook hoist that had to be
rotated out the way to clear the raised fork tower of the forklift.
When the hoist would be swing back, it would provide a convenient,
safe location to attach a block and tackle to dismantle the gearbox.
The gearbox was gently
lowered – and laid to rest on a pile of carefully selected wood
blocks to fit in alongside the sharply rectangular sump and hold the
unit stable. (Pic A26 below) We were then interrupted by
the Sunday train coming home and needing to be serviced. But
distractions aside, it wasn’t forgotten to mark off the open wheel
drop pits with yellow tape. (Pic A27 below.)
|

|

|

|
|
A25 – Somehow the gearbox doesn’t
look so big dangling form the forklift’s tines.
That’s the ‘Enchantress’ 25NC No.3488 in the
background. Notice how it looks as if the brake vacuum
line is neatly dodging Andrew’s head.
|
A26 – The gearbox is laid to rest on
top
of wood packing and under a half ton
hoist. It would be stripped in situ
during the following week.
|
A27 – Fred Sewell puts the finishing
touches on the barrier tape guarding the open pits.
|
|
SIA TASK : GMAM Garrett No.4079 ‘Lyndie
Lou’ – Bissel Axle bearings:
|
|
‘Lyndie Lou’s’
reconditioned Bissel truck has been sitting out under the traverse
workshop gantry crane for several months – just the teensy problem
of a missing axle being the hold up. Today the new axle
bearings were to be fitted. The donor axle had been mainly
stripped and cleaned several months ago, and stored with greased
journals. So there was little preparation between unwrapping
Lyndie’s new presents and getting them onto the axles. These
are NTN bearings, and cost R6000 per set of a pair of double taper
bearings. (Pic B01 below)
The conical inner race of the
old inner bearings had been left on the journals though and these
had to be removed. Because it’s backed right up against the
rear seal plate, the conical inner race alone cannot be withdrawn
with a puller and has to be split in order to open it up enough to
get over the axle journal. (Pic B02 below) Old ‘Swak
hart’ Viljoen did the first of the whole day’s worth of angle
grinding work. These bearing races are hard, and have a
healthy appetite for grinding disks. You can see a cut
progressing nicely in Pic B02 below, but can also see the problem
when the angle grinder disk reaches the rear – it would mean you
cut grooves in the axle box back plate. Thus, an angle grinder
was used to initially weaken the conical race, and then a chisel
driven into the groove towards the back plate to finally split the
race. These races loosened up without having to be broken
completely in half and could be withdrawn along the journal.
|

|

|

|
|
B01 – A brand new bearing and an
outer bearing race just taken out of the packing and so new
it doesn’t even have finger prints yet!
|
B02 – Dawie Viljoen cuts carefully
into the old bearing race as to not damage the seal housing.
This was the easy part of the job – the mallet and chisel
work was painful to watch.
|
B03 – A pair of split, scrap inner
bearing races, with a split inner spacer ring to the right.
|
Pic B03 above shows the
results – like an old experienced granny squirrel cracking nuts,
Dawie did a neat job of getting these races cracked. But Pic
B03 (above) also illustrates a problem. The inner race spacer,
shown on the right, also had to be split to get it off and these
don’t come in the bearing packs. Dawie had to re-weld, grind
and close up each one of the journal spacers that he removed.
Getting the bearings on
involved heating up the new bearings to expand them enough to get
them over the axle journal. This is a tricky operation
involving the carefully evenly spread application of an acetylene
torch – fitted with a heating nozzle. (Pic B04 below)
Not only does one have to heat the bearing evenly, but it is vital
not to overheat the steel - otherwise the tempering is lost and the
brand new bearing is basically scrap, as good as it still may look.
The usual way to judge the heat is by spitting on the bearing and
waiting for the saliva to start bubbling. That’s the ideal
temperature. If the saliva skitters on the surface or just
boils off, the bearing is already too hot and need to be allowed to
cool. The problem is that it is such a nerve wracking job that
the mouth goes dry and there’s often no saliva ‘on tap’ with
which to test the bearing!
It took Dawie three
hot-fingered attempts to try and get the bearing on, (Pic B05 below)
before he gave up and left it to cool on the old spacer and got up
in disgust. (Complaining about his ‘Swak Knie’ (Weak
Knees) ) Apart from the risk of burning your hands, even with
welding gloves – should the bearing cool down enough to contract
on the shaft and grip in the wrong position – the inner race needs
to be tapped off. The contraction problem is compounded if one
has put the bearing on skew. And even in a stubborn but
dead-straight application, the mass of the axle journal acts as a
heat sink, resulting in an undesirable cooling that speeds up
contraction, thus rapidly shortening the working time and making it
increasingly harder to put the bearing on. As big and as
robust as these railway axle bearings appear, it is quite possible
to wreck a new example before you even get it on.
|

|

|

|
|
A04 – Putting on the heat – a new
bearing is being expanded to be able to slip over the axle
journal. Notice it is resting on an old bearing race
and the flame is being carefully played as not to flare out
at the ends and penetrate the space between the roller cage
and the inner race.
|
A05 – Dawie tries to get the bearing
on straight before it cools down and contracts enough to
grip the axle journal. He wasn’t successful on
the first three attempts.
|
A06 – The torch was popping as the
nozzle had been changed for a general heating nozzle opposed
to the usual cutting nozzle – but the cylinders still
needed to be set up.
|
The job was enlivened by a
popping and misfiring acetylene torch, which wasn’t running
properly with the newly fitted general heating nozzle. (Pic
A06 above) When these torches mis-fire, they quite literally
pop and bang, startlingly loud in the echoing confines of the
workshop. Shaun ‘Smudge’ Ackerman got the torch to behave
eventually, without singing off his 4 day harvest of whiskers.
|

|

|

|
|
B07 – Polishing the axle journals
with extremely fine 1000 emery paper.
|
B08 – Cleaning out the gunk and old
grease
from the grooves in the back plate.
|
B09 – Impressive manoeuvring with
the LPG gas powered forklift. That is one of the
original GMAM axles, with badly worn flanges, being brought
in for stripping.
|
The advice of the Chief
Engineer was sought, and Andrew King toddled over from the next
track from where he was supervising the jacking of Class 15F No.3052
‘Avril’s’ tender. The Locomotive Doctor prescribed some
time doing more axle polishing and dressing. Dawie was just
able to get the bearing over the end chamfers on the journals –
which left some fine score marks. So Shaun Ackerman dressed
the chamfers on both axles with a fine file, while Dawie Viljoen got
going with strips of very fine 1000 grit emery paper to polish up
the axle journal. (Pic B07 above)
The cleaning and polishing of
the axle journal did the trick and the new bearings slipped into
place on the next attempt to heat and expand them. The next
challenge was to source a set of properly sized inner race spacers
as the existing ones had been split to get them off. In hopes
of finding a pair of freebies, the LPG gas powered Hyster forklift
was fired up and used to bring one of the original GMAM Garrett
axles from out the back lot and into the working area. (Pic
B09 above) I was surprised to see the forklift run as I’d
assumed it wasn’t operatable. I was impressed that in
managed to get over the track in combinations of forward and
reverse, and opposite steering locks. It didn’t hang up on
the rails and the differential didn’t trap the vehicle with one
wheel spinning idly in the air. I’ve driven forklifts before
– on a military job that required the use of forklifts as
self-propelled step-ladders in SADF ammunition bunkers.
They’re not as easy to drive as they look, especially with the
rear wheels doing the steering. Each one of us had a forklift
assigned to personal use … and I remember the forklift races…
But back to the present.
This original GMAM axle was the one that alerted us to the initial
Bissel truck problem on the Garret, with seriously worn and
sharpened flanges. As the axle was taken out of service, no
one had bothered to strip the bearings. And thus, the inner
bearing spacers were still in place.
Dawie got stuck in with the
stripping and the whacking to get the outer bearing dismantled
before the spacer could be withdrawn. It’s a brutal process,
requiring that the finely machined bearing cage be sliced through in
two places and literally levered apart until the rollers drop out.
(Pic B10 below) The inner race was removed by splitting it at
the top, and then hammering from the side, (3 o’ clock position)
with an apposing mallet held as a dolly on the opposite end.
(9 o’ clock position) The effect would be to crack the high
tensile steel – instead of going through the schlep of cutting
through the extremely hard material the second time. The inner
spacer was split and removed – and found to be of adequate length
to fit between the new bearings on the donor axle. However,
the split inner races had to have the cut areas cleaned up and
welded closed again. This was done with a grinder (Pic B11
below) with attention to not only grind the circumferential corners
flush, but to prepare the ends for welding. Welding was done
with an inverter welder and the loss of a few rods (which we found
when cleaning up at night) (Pic B12 below) Dawie found
the half-shell welding goggles a bit uncomfortable, but didn’t
take the chances of welding with exposed eyes.
|

|

|

|
|
B10 – An unavoidably brutal job,
ripping a defunct bearing apart to expose the inner race for
removal.
|
B11 – Dawie is grinding the cut slot
in a recovered bearing spacer, preparing the edges for
welding it closed again.
|
B12 – Welding the spacer closed
again – believe me, there is a work piece
in amongst all that ultra violet nimbus.
|
The bearings were assembled
on both ends with the newly fitted inner bearing race spacers.
The castellated locking collars were installed too, to snug
everything up to working pressures. But before these were
fitted, their castellated slots had to be cleaned and straightened.
(Pic B13 below) We had to use a mallet and wedge to get these
off, which damaged the working surfaces a bit. The railways
had a custom made tool for this wok – none of which we
Reefsteamers got with the depot.
Before the semi circular
outer race spacers were fitted into the screwed in bearings, special
care was taken to measure the distances between the outer bearings.
(Pic B14 below) At the same time, the outer races were pulled
flat against their bearing rollers and measurements were made at
various quadrants to ensure that the bearing has been put on
straight and true. (All measurements the same.) We used
an inside micrometer to transfer the measurements to a conventional
outside micrometer and got measurements down to two places beyond
the decimal. That GMAM has never run so straight and smoothly
as she will when we’re done with her!
The semi circular outer
bearing race spacers were individually cleaned up (Pic B15 below)
and measured as well, to be fitted to suit the gap.
Unfortunately, the axles, inner and outer race spacers and
obviously, the new bearings, have never been run together so very
careful matching had to be done.
|

|

|

|
|
B13 – Cleaning and dressing the
battered slots in the castellated locking ring.
|
B14 – Using an internal micrometer
to
check the space between the bearing races – for correct
spacing and to assess whether
the bearings were running true.
|
B15 – An outer bearing race spacer
before cleaning and measuring for selection to
suit the new bearing clearances.
|
The spacers were found to be
suitable for the axle at one end only. The spacer was laid
aside for machining. To get the job moving, Shaun fitted the
end locking plate that positively engages the castellated slots and
prevent the ring from turning loose. The originals had been
moved and possibly even dumped in the depot clearing project,
possibly by someone who didn’t know what they were. Shaun
found a pair of spares and fettled one of them to fit. (Pic
B16 below) the two lock-down bolts were cleans and lubed and
tightened right up. Then the bearing clearances had to be
tested once again to check that the relative spacing hadn’t
changed.
Shaun then began cleaning and
preparing the axle box, beginning with a good wipe down. The
working surfaces didn’t clean up too well and required some emery
paper to come up acceptably for intimate contact with our nice posh,
shiny, blingy new bearings. Two of the studs were missing and
some of the others were loose. Upon cleaning, both the axle
box (Pic B17 below) and the assembled bearing (Pic B18 below) were
coated in white grease. This will serve to protect the bare
steel while the axle is standing idle and the boxes have yet to be
filled up with grease.
|

|

|

|
|
B16 – You can clearly see the
vertical locking plate engaged into the castellated locking
ring at the 6 o clock position. Note the tea that I
brought in to distract the mechanic, so I could get a clear
shot! I = Sneaky!
|
B17 – The cleaned and greased axle
box almost ready for reinstallation except
for a few missing and loose studs.
|
B18 – There’s no more machined
steel bling as the protective ‘white grease’ is slapped
on.
|
Putting the axle box back on
required two people to guide it by the horn guides, one fellow to
guide it over the backing plate and one fellow to tap it on with
wooden block. This contraption is heavy and obviously rotates
freely on those bearings. The job was done quickly, but some
of the studs needed attention right behind the wheel which slowed
down assembly. So at least one set of bearings have been done.
The other set were measured once more and the semi-circular outer
bearing race spacers handed to Dawie for machining down during the
week. The open bearings were then slathered in delicious
onion-soup coloured white grease and wrapped in the plastic bag in
which the bearings came in the packing box.
We have the AGM next week,
followed by an arranged social ‘braai’ (BBQ) for the entire
club. Although no alcohol will be consumed by those who would
be working in the depot while the socializing is going home, it’s
likely that a morning of sitting and then stuffing oneself with meat
will have a soporific effect. We hope to get the axle fully
assembled with both sets of bearings and back into the Bissel truck.
Our plan is to run the GMAM Garrett No.4079 ‘Lyndie Lou’ on a
debut Magaliesburg run at the end of this month!
|
SIA Project – Class 15F No.3052 ‘Avril’
Tender Inspection :
|
|
Class 15F No.3052 ‘Avril’
stuck her cow catcher into the action again, or more accurately, the
tender. The fact that the brakes would never operate quite
right meant quite some time was spent underneath and checking the
running gear. The tender turned out to be in shabby condition
deep down below the newly braced and welded coal space. The
jacking was performed by Edward with supervision from Andrew King
– and some drilling concerning the use of sequential blocking for
safety in case a jack fails.
The brake rigging was found
to be rusted and misaligned. The under frames have much
surface corrosion and the packing between the frames and the water
tank is in poor conidtion. The tender was uncoupled from the
engine and jacked up at the front end. (Pic S01 below)
The front bogie has been removed for inspection. The bogies
are to be cleaned and sealed on all internal surfaces. The
brake rigging is to be repaired (Already underway) and the springs +
hangers are to be inspected. Each one of the triple axles are
to be individually removed, the axle boxes stripped and the bearing
sets checked for pitting and damage. Care will be taken to
mark and return the axle boxes back onto the axle journals from
whence they came. While the bogies are out, the sections of
the tender’s framing above and around the bolster pins will be
scraped back and cleaned.
The interconnections between
the engine and the tender include, from left to right : (Pic So2
below)
1). The LHS injector
feed-water pipe. (Feed from tender’s water tank)
2). The LHS safety chain.
3). The McLaughlin joint
equipped mechanical stoker motor steam supply line.
4). The draw bar withdrawn
right from under the buffer pad. (Which operates with an
Inter-cushion Buffer.)
5). Ascending Stoker Worm.
(Pic S03 below) – it just slips out the tunnel.
6). The flexible
claw-coupling fitted exhaust pipe for the stoker motor. (It
discharges into the ash pan.)
7). The train brake vacuum
pipe.
8). The RHS safety chain.
9). The right injector
feed-water pipe. (Feed from tender’s water tank)
10). The electrical
connection to the tender lamps. (Under the cab roof)
|

|

|

|
|
S01 – An ex-Class 23 EW-type tender
adopts a sit-up-and-beg attitude with the back end safely
chocked and the front end on blocks and jacks.
|
S02 – The naked looking back view of
a Class 15F’s cab. Can you identify all the
connections according to the list above?
|
S03 – Above the inter-cushion
buffer, the ascending stoker worm droops pathetically
outside its accustomed tunnel. Notice how shiny the
uncoated steel surface is from being polished by the
abrasive coal.
|
When both of the bogies have
been overhauled and are back under the frame, the entire tender tank
\ coal hopper is to be lifted off the chassis to repair and replace
the decking as necessary. The entire rolling chassis will be
then stripped back, carefully inspected for cracks and rivet
failures, repaired if necessary and then given a good thick coating
of water proofing. The tender tank underside will be stripped
back and inspected for weak points and weeping type water leaks, and
reinforced where necessary.
We plan to have the steam
crane properly re-certified and back into steam by then, and so
we’ll have ‘Shosholoza’ back to full strength to help hoist
the tender body around off and back on the frames again.
Essentially, Class 15F
No.3052 ‘Avril’ is going to be treated to a full tender
overhaul. Following are some photos that show the existing
condition.
|

|

|

|
|
S04 – Visually, the frames look okay
but we can only check them properly once all that gunk and
rust has been removed. That’s the train brake vacuum
line passing to the RHS.
|
S05 – Corrosion is evident in some
of the
web plates under the deck packing. This
is the tank valve for the RHS injector.
|
S06 – Looking back towards the brake
vacuum cylinder. If the decking fails
between the tank and the frame, it encourages rust and local
damage
from metal-to-metal contact and friction.
|
Someone might pick up that
this 12 wheel tender is technically incorrect for the SAR Class 15F
type locomotive. They would be correct too ... many of the
Class 15F’s were retro-fitted with the longer Class 23 type
‘EW’ tenders to extend their operational range. (Pic S07
below) The large Class 23’s, slightly bigger than the 15F’s,
were all retired as a class in the early 70’s because of
widespread metal fatigue in their 5 inch thick frames. This
was their heritage from being built with second grade German steel
at the onset of WWII, while the best steel was reserved for the
armed forces. The SAR Class 15F’s were originally fitted
with short 4-axle tenders (the JT type) to fit on turntables.
(15F No.2914 ‘Spikkels is still running with a ‘short’ JT
tender.)
The original 4 axle JT type
tender carries 14 tons of coal and 21 280 liters of water. The
longer (and visually much more appealing) EW type tender carries, by
contrast, 18 tons of coal and 35 970 liters of water. The
longer tender is considered much more attractive as it lengthens the
tractive set and visually balances out the engine. A
disadvantage is the center axle seriously restricts access to the
bolster pivot clamps and the brake relay rods. (Pic S08 below)
These are usually serviced once a year and the bogies have to be
dropped to do this. These ones haven’t been taken off for a
long, long time. Incidentally, the 6 axle tenders for the
Class 25 series, condensers, converted and conventionals, all share
the same weak point.
|

|

|

|
|
S07 – A triple axle Class 23 tender
bogie.
|
S08 – The opened bolster clamp ring
– which had to have the bolts cut to release the bogie.
You can see the four relay rods for the brakes, which cannot
be reached for lubrication above the center axle.
|
S09 – This type ‘EW’ tender has
four
brake shoes per axle, making 24 brake
shoes in all and 12 brake rods
servicing 6 axles. We’ve started stripping and
servicing the rods and the shoes.
|
|
SIA PROJECT : GMAM No.4079 ‘Lyndie Lou’
Stoker Motor Replacement :
|
|
It was high time to clean up
the big dusty doll parked on road No.4 in the Workshop. We had
hoped to get the Sandstone Estate’s GMAM Garrett No.4079
roadworthy in the early months of this year, and were even talking
about some sort of launch or unveiling on a summer time Magaliesburg
run. However, Dave Shepherd’s Class 15F No.3052 ‘Avril’
rolled on her then-bulls eye wheels into the limelight and kept us
occupied for quite a few weekends.
But ‘Lyndie Lou’s’ time
has finally come around – and she IS actually to be cleaned and
polished this week! Actually, the engine is quite clean in
terms of oil and road dirt, and even has some new detailing paint
– just the dust and cinders from the shed have collected a bit.
The repair work would involve rebuilding another axle to enable us
to get the rebuilt Vesconite-equipped Bissel truck back under the
engine where it belongs. The overhauled Stoker Motor was also
properly reinstalled. It had been slinged into its recess a
week ago, on the leading RHS corner of the rear bunker. So it
simply needed to be nudged into its final position and connected up.
Mike Thiel did the refit
work, appropriately, being the fellow that rebuilt the contraption.
It took him the whole day – wasting time because of poor access
and having to contort himself around and even behind the stoker in
its recess. He reminded me of a flea getting into a dog’s
ear. Because of the close confines and poor lighting, it was
hard to take decent photos – but there’s enough for you to see
the process.
|

|

|

|
|
T01 – Michael starts the job by
removing the hoisting strap. This cramped working
position would be typical for his Depot Day. The water
separator is clearly seen to the right.
|
T02 – The stoker steam exhaust
coupling
that was the first task of alignment.
|
T03 – A Michael-free view of the
stoker’s steam intake piping, clearly shows the
‘slight’ misalignment problem. The thin copper
pipe to the right is the lubrication line.
|
The job started by removing
the sling strap. (Pic T01 above) The stoker had been
dropped squarely onto the mounting pads, but the foundation bolts
had not yet been fitted. It could be shifted slightly and
lifted upwards to get the strap out. But in Pic T01, you see
how the hoisting strap managed to tangle up with the exhaust line.
Michael’s strategy was to
get the two largest pipes aligned, being the steam inlet and the
exhaust, before snugging down the foundation bolts. (Pic T02
above) The small bore lubrication pipe could be bent to fit,
and the drive shaft runs with universal joints anyway, and can
naturally take a bit of misalignment. Of the two large pipes,
the exhaust pipe was the most rigid and would cause the most
problems with leaks at the union, albeit with exhausted
non-pressurized steam.
It took some close quarter
grunting to rotate the stoker motor and shift it outward to line up
the pipes. The male threads received a seriously generous
helping of graphite grease before the union was started and
tightened up on the first few threads. The next task involved
rotating the badly misaligned steam intake pipe with the intake.
(Pic T03 above) You can see that this intake is complete with
its choke valve and bleed nuts. All locomotive oil lines that
fed into a pressurized steam space, typically the stoker motor,
valve chests and the cylinders, are equipped with chokes
(restrictors) to reduce the effective force of the pressurized steam
blowing back up into the lubrication lines. This stoker intake
also has an intact bleed valve – a facility to physically open the
line and see if oil is actually getting into the steam intake.
Whether on a tender locomotive or a Garratt, the Mechanical Stoker
Motor is fed by a long and vulnerable oil line from across the
yawning gulf of the tender drawbar, and ultimately from the
Hydrostatic lubricator, or the eccentric-driven mechanical
lubricator up front as the case may be. The top nut on the
brass fitting is to allow direct injection of oil. A
mechanically lubricated locomotive does not generate pressure in the
oil lines when at stand still. While that doesn’t hurt the
pistons and the valves as they are naturally at stand still, the
stoker may still be in use.
Anyway, this fitting would
have been easy to rotate anticlockwise to line it up – but that
might cause leaks as one would loosen the pipe threads. With
this in mind, Michael grunted it around clockwise to line it up,
with a gwala bar inserted into the tee-piece. Clockwise is
tighter – hence the grunting and the gwala. He managed to
rotate the intake into line without stripping the threads or
cracking a pipe (Pic T04 below). The steam intake got the
brushed-on graphite grease treatment on the threads, and just like
the wider (low pressure) exhaust pipe, the union was run up on the
first few threads.
The oil line received the
same treatment (Pic T05 below) before the task of gently snugging up
the foundation bolts to ensure the alignment stays intact.
Getting the bolts down evenly was the most contortionist of the
jobs. I was watching Michael from my vantage point from
underneath the green critter in the next track – and sometimes you
might just see one grimy arm and a pair of blue clad buttocks
elevating like a noon cannon.
|

|

|

|
|
T04 – A view of our stoker-boy
through the rear RHS cab window. He looks grumpy
here, but that’s because he’s concentrating and also
trying to keep his balance – he’s usually one of the
most cheerful and
gentle of the Reefsteamers family.
|
T05 – Connecting the oil line.
Mike’s elbow is on the automatic water separator –
necessary to eliminate the condensate that forms when the
steam cools in the long line from the Turret valve in front
of the cab, all the way to the stoker out back.
|
T06 – Polishing a long unlubricated
universal joint spider with 1000 grit emery.
|
The Universal joint looks
like it hasn’t seen oil for several years – but the ‘spider’
and the universal joint yokes were still serviceable. There
was light surface rust but no real pitting. Michael took the
spider and polished each of the four ‘legs’ (Pic T06 above)
right down to 1000 grit emery. The compound yokes were
externally brushed off and the bores cleaned out. You can see
the newly cleaned and lightly lubricated spider next to a roughly
cleaned yoke plate in Pic T07 below. This was dark and
restrictive work (Pic T08) The engine had to be turned to get
the lower yoke plate horizontal to act as a shelf to hold the half
assembled joint on the square-sectioned primary shaft.
|

|

|

|
|
T07 – Parts of a GMAM stoker
universal joint. This is a cleaned spider next to
roughly cleaned yoke plate. These plates work in pairs
– making four plates to form one universal joint.
|
T08 – Reconnecting the stoker shaft
– you can just see the universal joint. That weirdly
floating torch has become a Michael Thiel trade mark – it
has a strong magnetic clamp but looks weird in 2D photos.
|
T09 – Tightening unions is a boring
job, hence the yawn. Mike is still doing the hand
tightening before using the green headed mallet visible on
the footplate. It’s a slogging spanner, designed for
such use.
|
With the shaft tightened up,
the foundations bolts creaked into place and the pipes lined up, it
was time to do the finishing work of tightening up the steam intake
and exhaust unions respectively. They were easy to line up by
hand as the well-greased threads had already been started before the
stoker was bound-down. The slogging spanner finished off the
job – one hex at a time. This stoker motor has been test run
on compressed air and it was assessed to run powerfully and smoothly
after a thorough strip n’ rebuild. So the GMAM Garrett
should be able to feed herself for years to come, and unlike certain
rail operators, we will take care to keep the vulnerable universal
joints lubricated!
|
PROJECT : The Chairman climbs in :
|
|
The ‘Cute Chairman’ Elize
Lubbe came high-striding in between the biggest and the littlest
green machines, apparently quite dissatisfied with the acetylene
torch techniques of the crew. She climbed right in to
demonstrate just how to cut a slot in an axle bearing race.
The results were hilarious.
|

|

|

|
|
U01 – Getting ready to kick some
butt,
a businesslike Elize dons her hard hat
before terrorizing us in the Workshop.
Incidentally, the hard hat requirement
is enforced for all visitors, and all non-workshop-based
Reefsteamers personnel.
|
U02 – Now this, Ackerman and Viljoen,
is how to cut up a bearing race
and look elegant while doing it.
|
U03 – Er, Elize…. Those
goggles are to protect your eyes, not your nose!
|
|

|

|
|
U04 – The powder-puff girl.
Someone should tell Elize that locomotive grease is good for
the complexion. (Because once you’ve scrubbed it
off, you’ve removed the top layer of skin anyway –
automatic exfoliation.)
|
U05 – Which one is the flower?
Elize prances about after a successful
flower delivery for the new club house.
|
As you can probably tell,
these pictures were posed. Elize is a good sport and wasn’t
annoyed when we asked her to participate in the workshop. She
is an effective and tireless campaigner for our cause. She is
obviously distinctly out of place amongst the tools, big chunks of
rolling iron and the grit, but is definitely in her element with the
phone, fax, computer and the A4 paper. (Those finger nails
wouldn’t last very long for sure and they’d take forever to
clean, but they WOULD: be useful as built-in gasket pickers.)
She isn’t dykish or mannish in her demenour, still maintaining her
femininity in what is definitely a male dominated world. She
has earned maximum respect from each one of our regular members.
Without Elize representing us and sometimes quite literally striving
for us, this Steam Locomotive Association would be going no-where
fast.
|
PROJECT : Club House :
|
|
The new Clubhouse (ex
ablution block) has made great strides and is almost finished –
Fred Sewell has worked his buns off on this project and the results
are well worth it. In the mean time, the existing clubhouse
has had some work done in terms of clearing up and organizing – a
project driven by none other than ‘The Cute Chairman’ herself.
The idea is to use | |