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Reefsteamers Depot News Report
- Weekend, 01-02 December 2007 -
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Introduction :
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FP01 – I hate mornings! But some Steam
Action is always worth getting up for. And if
you have been minding locomotives overnight, you get first pick of the
morning photographs.
The guys were in a hurry, but I was lucky enough get this smoke deflector
and cylinder
glint shot as Class 25(NC) No.3472 ‘Elize’ backs into the yard from the
morning coal top-up.
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Another deceptively quiet weekend passed at the Reefsteamers
Germiston Depot as we once again had a day trip train running on both Saturday
and Sunday. Not including the catering staff, we usually have a crew of
about 8 depot \ workshop people on board the train(s), and a depot person
that come in later in the depot workday, as to be awake for a night shift of
Locomotive Minding on Saturday Night. (And we ask a volunteer to tend the
engines on Friday night too – a graveyard shift after a day at work.) However,
while it slows things down a bit at the depot in terms of workshop manpower –
this is Steam in Action, rolling out the miles on the rails and
earning some revenue.
Saturday’s day-tripper train was another successful train
as arranged by SANRASM (South African National Rail and Steam Museum) and it ran
to Magaliesburg with over 440 passengers on board! It was reported as being
a sprightly run, with the Class 25(NC) No.3472 ‘Elize’ just playing with her
train. Good timings were made on the trip home with clear lines and green
lights all the way.
Sunday’s train was also to the Magaliesburg area, but
actually through Magaliesburg Station and beyond to the private stop of
Swallows Inn. The entire train was booked as a company function but only
about 3 coaches of the 10 vehicle train were in use. The magnificent 25(NC) took
the load like a shopping trolley full of helium balloons. There were a
number of halts and a wait for a train load of crushed coal at Magaliesburg
that spoilt our timing a bit.
Back at the depot, we had six people for the day, including
our resident videographer. The speedometer drive as well as the lubrication
components was re-installed on the newly overhauled and re-installed Bissel
Truck under the Sandstone Heritage Trust’s GMAM Garratt No.4079 ‘Lyndie Lou’
The removed Bissel Truck from the trailing engine unit was parted from it’s
axle and placed into storage, the axle to be serviced and used in the frame
of the donor Bissel. Work continued on the grease pad press as well as the
fabrication of more Vesconite bushes for the Class 12AR No.1535 ‘Susan’. Andrew
made progress on the axle pad grease press.
But … on with the detailed reports!
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PROJECT – Finishing up the GMAM Garratt Bissel Truck :
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FP02 – Zero to sixty in two weeks?
Sandstone Heritage Trust’s GMAM Garratt No.4079 ‘Lyndie Lou’ is
almost ready to run under the Steam in Action banner and we plan to run
this engine on the 17th December.
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We’re under a bit of pressure to get the ‘big mean green
machine’ aka the GMAM Garratt back in steam for the 17th
December. (Post edit – Actually the 15th December for a test
run) Steam in Action is about getting things done, but the schedules and
requirements of a national steam preservation and coordination programme will
certainly chivvy the individual clubs on a little bit. With the benefits of
having clear goals, commitments and incentives come the deadlines, but a bit
of stress is good and sorts out the priorities. The donor Bissel Truck needs
to be reassembled with the new Vesconite slide bearings installed, and the Bissel
Truck itself put back in under the frames. The bolster plate and swing links
are ready and waiting. The axle from the Bissel Truck that was removed last
week (trailing) will be used in the donor’s frame.
Meanwhile, the stoker motor is to be re-assembled and
reinstalled. The crankshaft, and the crankshaft bearings have been prepared
and the big end bearings have been scraped to suit. A surprise job that came
up was the discovery of a broken spring on a driving axle – so that needs to
be replaced as well. All this in two weeks! There are some week nights of depot
work coming up.
There’s always the detail work to be done on a major
project and the Bissel Truck re-assembly was no different. Shaun ‘Smudge’
Ackerman attended to the re-mounting of the speedometer drive, which is on
the RHS axle end of the leading Bissel Truck. Simultaneously, ‘Nippies’ Juan
reassembled the lubricator cups and the pipes.
A typical speedometer drive on a South African Railways steam
locomotive looks rather like the gravity driven odometer drive that one sees
on the hubs on many trucks and busses. (Pic F01 below) Much larger, of
course, as everything is with the elephantine engineering of steam. However,
this is an electric device, the rotation of the wheels spinning a magnet to
generate an electric current in a set of windings, the amount of current
being proportional to the speed of the engine. These speedometers work in
both forward and reverse.
The speedometer drive is via an off-set pin that engages in
a claw. The speedometer drive itself is a sealed unit and is a modular
design, able to bolt onto any standard Bissel Truck’s axle box. Pic F02
(below) shows the drive pin. The first job was to clean out the battered and
dirty threads in the axle end. The first challenge that came up was that the
original drive pin was too short and not engaging in the claw. It’s the
typical problem faced when working on half-century old locomotives where
parts have been swapped, refitted and plain simply bastardized – not much
standardization remains. That’s why the trade is called FITTING and
turning.
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F01 – General view of the Bissel Truck.
You can see the speedometer coupling and the cable on the concrete workshop
floor. Notice that the lubrication gear
has already been installed.
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F02 – Internal detail of a speedometer
drive coupling. This is a rare and exotic shot
as the interior of the speedometer cup is common to the axle box cavities
and is usually full of grease.
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F03 – Shaun uses a try square to measure
the depth beyond the axle box flanges.
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So a bolt had to be scrounged to fit the drive pin’s newly
rethreaded hole and then cut down to suit after measuring the depth required
to drive the speedometer. (Pic F03 above) This required 2 measurements
– the depth down to the axle end and the depth of the speedometer drive cup.
Shaun did the job with an engineer’s try square as a depth gauge and adding
the figures together. However, he also had to allow
for the depth of the threaded portion as well.
A round headed bolt was scrounged, screwed in to the axle
end and then marked with the required depth.
The bolt head had to be cut off at the mark, requiring some close quarter
sawing work from the wrong side.
(Pic F04) Shaun had the hacksaw set as standard, cutting on the forward cut,
so he had to crouch on the left side, awkwardly under the steam lines, to
have the forward cut tend to tighten the bolt clockwise rather than loosening
it. Shaun also had to crouch down under the characteristic steam transfer
lines of the Garratt
(Pic F04 again) and his brand new hard hat is already bearing many marks and
scuffs.
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F04 – Cutting down the speedometer drive
pin. Notice that Shaun is cutting wrong handed as to have the cutting
stroke
of the saw tend to tighten the bolt.
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F05 – It is just not done to have the
speedometer fall off the locomotive!
Poor show! Here we see the Speedometer’s generator casing being carefully
torqued
up to the drive casing.
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F06 – The plain end of the Bissel
Truck with lubrication hardware mounted and the pipes aligned to the axle
box horn guides.
The pipes will be removed during painting.
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After filing down the rough cut end of that bolt, the
speedometer drive went together with little trouble.
The flange bolts had to be torqued carefully in sequence as the mating
surfaces aren’t quite square.
The bolts holding the speedometer assembly together were also tightened up.
(Pic F05 above.)
Meanwhile, Juan was putting the lubricator cups and the associated
drip feed piping back on the opposite axle end. (Pic F06 above) He’s a very
quiet, speedy worker and we were hardly aware that he was there. He faced
his own challenges though. As per the loss of standardization for the
speedometer coupling drive pins, the standardization for the oil cups and
their pipes was lost long ago. This is especially true as the removed and
cleaned parts were all put into one box to be locked away safely in the brass
store. Juan had to tweak the pipe brackets to fit, clean some threads, and
bend the convoluted, somewhat battered copper pipes to optimize the
lubrication to the sliding surfaces of the axle box horn guides.
It may seem a little odd that we’ve had all the lubrication
hardware mounted on the frame
before the Bissel Truck gets painted. (Pic F06 above) What we’ve done may
seem analogous
to putting a light switch’s face plate on before painting a wall, and then
trying to paint around it.
However, the odd job sequencing does have a reason. The
mechanical people prefer to do their own work from start to finish. Those oil
pipes can be removed temporarily to paint neatly behind them – but at least
it is known that they and their brackets actually fit. It is planned to have
the Bissel painted black by the pensioners this week.
So that’s one Bissel Truck done and one to go! Now we just
need to work out the terms of Warrantee!
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PROJECT – Dropping an axle on a GMAM Bissel Truck :
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We knocked off for lunch at about 2pm – fish n’ chips and Russian
n’ chips, simple, solid food upon which locomen thrive. And the Russians
usually have enough grease in them to do up both sets of cross head
slides and have enough left over to seal the smoke box ring! We were disciplined
enough to get back on our
feet just as the summer afternoon nap-attack was sneaking up, and we settled
down to dropping the axle from the removed Bissel Truck. However, this
wasn’t without a serious and vital discussion of allocated nicknames and the
addition of glasses, horns and moustaches to the mug shots on the bulletin
board.
Actually, Andrew ‘Noddy’ King and Paul Hloben had already rolled
the Bissel Truck along the trolley tacks, trussed and hung the Bissel Truck (Pic
D01 below), while Shaun and Lee went on the road house food run.
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D01 – Hung like a dressed turkey,
the old GMAM Bissel Truck is tipped back
to expose the four span bolts, two across
the axle cavity and two under the axle boxes. The stripped locomotive in
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background is Class 12R “Rosie.’
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D02 – Lacking only whips to spur them
on, the Bissel Boys do a bit of capstan work to ‘crack off’’ one of the
span bolts’ nuts. Notice that Paul Hloben (Right) is already letting go of
the cheater tube in case the nut lets go and the tube swings into the grey
‘Komati’ box.
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D03 – A locked nut. No, a locked
wheel.
No, a locked bolt. The old fashioned style spoked wheel comes in useful to
lock the spanner on the very last span bolt.
The black vertical cylinder above
the spanner is the spacer sleeve.
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Dropping a Bissel Axle isn’t all that difficult a concept,
involving the removal of the four span bolts and lifting the frame off the
axle. This unit was filthy and it was hard to tell the bolt ends from the
nut ends under a uniform rounded coating of dirt. Fortunately, the Bissel
tipped over like a dead bull – that is, nuts up. Three of the span bolts
came loose reasonably easily with Shaun Ackerman, Fred Sewell and Paul Hloben
doing capstan work with an old boiler tube as a cheater bar. (Pic D02 above)
Each bolt was held in place with properly tightened double nuts and each one
required properly expressed grunting to get them off.
Shaun had the unenviable task of bucking all that leverage
with only a spanner, and was finding inventive
ways to block the spanner from turning. He managed without getting of his
fingers trapped. (Pic D03 above.)
But the third span bolt was a bugger, sticking tighter than
an ANC politician to their version of a court testimony. (Pic D04 below) You
could see the quality and craftsmanship of the dismantling work degrading in
the increasing desperation of trying to get that bolt out. First some civilized
tapping with a four pound hammer, which became full armed swings.
Fred ‘Sparky’ Sewell went into Wiley Coyote mode after
using a piece of scrap steel as a spacer to protect the threads – the shock
and vibration running right up his arm and fusing his central nervous system.
The pieces of scrap timber that we tried just bounced or otherwise dented
under the load. (Pic D05) Then the heavy mallets came out and it became a kinetic
energy carnival – three swings to the dollar. We gave up on preserving the
nut and eventually on the threads.
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D04 – Three out of four isn’t bad for
a test, but spells absolute failure for a Bissel Truck rebuild. The jammed
bolt is the one that is second from the left – with the other three bolts
all submissively loose and their heads
resting at ground level.
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D05 – Still in the refined and
correctly techniqued stage of the attempted removal –
a wood block is used to try and protect the nuts and the span bolt’s
threads. It wasn’t successful, just bouncing futilely off and absorbing
the energy from the hammer.
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D06 – Fred nervously holds the drift
with a ring spanner while Shaun cranks up for another fusillade of blows.
It was as awful lot of energy expended for less than an inch of motion.
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With all the hammering, the bolt slowly turned and we could
soon see why it was ‘sticking to its point.’ The bolt is bent. Great. With
much hammering and surprisingly self depreciatory good humour (and equally
surprisingly little swearing), the recalcitrant bolt was drifted down to the
pad and then no more. It seems as if the head was spreading under all the
hammering and the stupid bolt was getting tighter all the time.
What happens when an irresistible force meets an immovable
object? The acetylene torch comes out.
As I said, you could see the degrading of techniques from
refined hammer taps, to lusty whacks and blows
to the point of last resort. You could almost see the locomotives wincing at
the sight of the cutting torch.
The baulky bolt and its sleeve were cut through in short order and
fortunately through the bent section –
the halves coming out with absolute and ridiculous ease after the fight the
bolt had put up.
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D07 – We reluctantly resorted to the
acetylene torch, cutting through the
bolt and the trapped spacer sleeve.
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D08 – The defeated bolt and the
truncated sleeve came out with absurd ease … a few taps with a drift and a
very welcome clank as it hit the ground.
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We didn’t even knock off for a well deserved cup of tea,
but used the pneumatic hoist to gently lift the hanging Bissel (with the axle
boxes temporally pinned by their bolts put in the opposite way, heads
retained by gravity.) As mentioned in a previous newsletter, the weight of
the Bissel is very close to the crane’s rated working load. The hoisting
cable is getting a bit frayed too – so we took care to just lift this big
lump off the ground enough to rotate it 90 degrees and put it back down
again. We then wanted to let the hoist cable out, and traverse the hoist at
the same time to guide the A-frame safely down to ground level. That’s when
we discovered that the chain has come off the traversing pulley. (Pic D09
below) So, we used ourselves as highly skilled paper weights to guide and rock
the Bissel Truck down with the hoist cables being carefully allowed to hang
diagonally.
We deemed the hoist to be located centrally enough to be
able to lift the frame. We then set up a three way sling with our
‘octo-chain’ and the cable sling, and withdrew the last two span bolts under
the axle boxes. We lifted the Bissel Truck frame carefully to disengage the
coil springs from their crowns. The process went well, but because of the
offset hoist, the a-frame was nosing up first and thus forming an
asymmetrical load. (Pic D10 below)
We also had to use crowbars to ease the axle boxes out of the slides, but
whether that’s due to a distorted frame, misaligned horns or simply the tilt
of the hoist is unclear. The axle initially tried to tip back, but we kicked
the boxes and pushed the Bissel forward and caught the springs with ease. (Pic
D11 below)
We then let the Bissel Frame hang while Lee Gates and Paul Hloben
were dispatched to find
a ladder long enough to reach the gantry, so as to reseat the traversing
chain in the hoist.
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D09 – The ‘derailed’ traversing chain
of the pneumatic hoist. Not the nicest discovery when you’ve already got 4
½ tons hanging from the hoist. Fortunately, re-fitting the chain was a
simple task.
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D10 – With the hoist off-center (hence
the nose-up tilt) we lift the frame off the axle. Here, the coil springs
have just disengaged from their crowns. We used crowbars to ease the axle
boxes out.
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D11 – The Bissel Frame disengages
and swings freely.
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You stand a better chance of finding a green Class 6E1
parked in our yard than finding a ladder – but we
found a nice long fiberglass electrician’s ladder. The traversing chain went
back on the pulley with little trouble.
We moved the Bissel Frame to a storage spot between two tracks with two men
guiding the heavy frame, two applying traction to the traversing chain and
one applying light tension to the slack to keep it between the pulley flanges.
We managed to get the Bissel Frame safely horns-to-the-floor without hurting
anyone or cracking the concrete slab.
This frame is to be retained as a spare and no work is to
be performed on it. It is planned to remove the richly encrusted muck off
the bolster plate and to soak the seized slides in diesel to free them up.
The solid brass axle horn guides are to be removed and put into safe
storage. The axle is to have the bearing boxes stripped and inspected – it
is planned to use the axle and it’s bearings in the donor Bissel frame as the
donor’s axle ends and bearings are damaged. We’ve got two weeks to get the
donor truck overhauled and back under the locomotive where it belongs!
Steam in somewhat frenetic action!
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PROJECT – New Axle Pad Grease Press :
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Andrew ‘Noddy’ King spent the day on his current project –
which is something a little different. Instead of convoluted, highly
technical work on a steam locomotive, he’s working on a custom fabricated
grease press.
We use these devices to press hard grease into semi circular perforated
backing pads – and the half round grease pack is used on the journals of the
locomotive axles. (Except for the 25(NC), which uses roller bearings.)
Today’s project was the fabrication of the sliding grease gate.
After double checking the ¾ inch steel plate for size, Andrew started by
marking up and slow-w-w-ly drilling out the rounded ends of the grab handle
holes.
(Pic G01) It required patience and much oil. The job was managed without
breaking the bit or revolving the work piece.
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G01 – A multi-tasking automatic
lubricator at work. Andrew feeds in the oil and the bit as he drills out
the rounded end of the grab slots.
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G02 – The grab slot is being cut
between the two drilled holes. Notice the scrap metal as a combination
ruler and shield to keep the slot straight.
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G03 – Cooling down on the trolley, the
raw edged grease gate shows its grab slot.
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The grab handle slots were cut through with an acetylene
torch. (Pic G02) A porter’s trolley formed a handy workbench in front of
the tool store, especially as the acetylene cylinders are such a drag (pun
intended) to move around the depot. The game plan was to make two cuts
between the drilled holes to form the outline of a grab handle. The top
surface had to be shielded with scrap metal to guide the edge of the cutting
torch’s flame. Andrew wisely let the plate cool down before moving it – and
ended up getting sucked into the work of the Bissel Boys.
But Andrew got away and disappeared to the corner vice where
the angle grinder was used to round off the raw edges and corners. Then the
operations were transferred to the corner shop where the grease gate was
cleaned up some more as well as the slots and back plates on the grease table
itself. The project ran out of Saturday during the mark up and cutting of a
backing plate for a pneumatic valve to operate the cylinder.
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G04 – Setting up some power in the
back shop. This is the custom fabricated grease press with the recently
installed cylinder.
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G05 – The reason for this new grease
press. A bin load of empty axle pad formers await re-greasing, and there’s
even more inside! We normally pack these in bulk and then wrap them in
thick grease-proof paper for storage.
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PROJECT – Class 12AR Valve Gear Overhaul :
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Work continued on the fabrication of new Vesconite bushes
for the Class 12AR No.1535 ‘Susan’.
This locomotive is out of action waiting for seven new
boiler tubes which are on order. We didn’t even waste our time with an
official boiler test, for although the tubes weren’t leaking as yet, they
were thin and wasted at the firebox tube plate end. This old girl awaits
re-assembly and boiler testing alongside Class 15F No.3016 ‘Gerda.’ We are
trying to arrange to have both the locomotives tested on the same day as to
only have to pay one set of call out fees for the boiler inspector.
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J01 – James at work, sporting his
pristine new hard hat. We are planning to eventually move this workshop to
a more centralized area.
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J02 – A newly fabricated lifting link
pin being test fitted. The horizontal bar is the radius rod, complete with
the square die block on the right side, which runs up and down the
expansion link. James is machining bushes for the pin – which connect the
lifting link to the way-shaft crank.
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J03 - A Vesconite Bush in the lathe.
Behind the rear collar (which is the original tube stock diameter) is
another thin section. James inserted the actual lifting pin, visible in
the center of the lathe chuck, to stop the thin walled bush collapsing.
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The valve gear bushes are almost complete. The next stage
of the Class 12AR project will be the
fabrication of bushes for the valve spindle bearings and glands, as well as
those for the pistons. Because
of the heat and pressures involved, these will be machined in traditional
bronze instead of Vesconite.
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Pictures from our Sunday Run to Swallows Inn.
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I’ve (Lee Gates) have included some pics of the Sunday
run. I was the locomotive minder for Saturday Night and thus took the
opportunity to sneak a snooze in an empty compartment before possibly getting
evicted by booked passengers boarding at Boksburg East. (It’s happened to me
before.) I didn’t nap much, not with the wonderful beat of a mighty Class
25(NC) just one coach away, but I didn’t take photos either. And when I did
rouse myself to walk through the coaches, I discovered that my camera
batteries were flat, and I’d left my reserve batteries in my briefcase back
at the depot. Fortunately, ‘Die Ander Elize’ (Alet) lent me some batteries
to take some pics of our stop over.
We had only had about 2 ½ coaches full of passengers and
the day sitters mainly ran empty. Looks as if this company’s function wasn’t
very well attended. We spotted the train in the country and the team split
into three. The girls, Lex and myself went to a local store for cool drinks
and to look at country curios. The loco crew went out on a hunt, to bring
home the braai meat and ended up hooking a ride on a donkey cart!
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S01 – What could be better than
setting up for a braai with your friends, on a mild summer’s day in the
quiet, green countryside – with a steam locomotive simmering in the
background? That’s Andre van Dyk’s Bakkie and he’d driven to the spot to
fire the Class 25(NC) on the way back.
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S02 – Tony ‘Shaky’ King rattles his
way from the power car’s kitchen with six glasses for coke. Tony has
Parkinson’s disease and
is a bit too fragile for heavy workshop work. However, he has found his
place of Action by training as combination Train Manager \ Safety Officer
and serves regularly on coach crews.
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S03 – The cute chairlady, Elize Lubbe
gets arrested and escorted into the paddy-wagon while Alet makes a run for
it. Bail was posted at 50c but no one would come up with it.
It was all in good fun but the police
were genuinely surprised to see us camped out on the road, next to the
train, in the countryside.
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We had a decent afternoon with a quiet braai and sitting in
the shade of the trees. We had to leave early though, as we had further to
run, and needed to turn the engine around as well. With beautiful timing, we
had to leave as soon as the meat was cooked – so we nibbled on the train and
the crew were chewing chops in the cab. The departure was enlivened by a
drunk fellow chivvying his equally drunk wife along with a stick whipped
against her ample backside, like whipping an ox along. She naturally
objected to this treatment and they laid into each other but were too drunk
to do any harm. I wondered if they even noticed the audience watching from
the train’s windows and doors.
We had a reasonable run back but were running late with
several delays and the locomotive turning. We got the passengers back at the
Boksburg East Depot at about 6:30pm, and were already closing the windows and
cleaning the trash in the coaches on the way home. There were water problems
back at the depot on Sunday – but when we arrived, there was water laid on to
service the engine and wash out the ash pans before our traditional after-run
cup of tea.
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S04 – Sweet Tannie Dorie Steenkamp
quietly watches over her family – innocently not knowing that she was just
minutes away from fending off the attempted insertion of a glittery purple
vibrator into her right ear!
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S05 – The first steps of fireman
training – how to handle a braai fire! Senior engine driver Oom Attie de
Necker shows a young first-time volunteer how to handle a braai fire.
Notice that Oom Attie is wisely standing where the smoke ISN’T !
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S06 – A grand, dignified old lady is facing
tender forward and simmering quietly while the humans, well, act human.
The engine was turned at Magaliesburg.
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S07 – Passengers boarding after a
great afternoon. Driver ‘Smudge’ Ackerman had
to lean on the whistle several times before they started coming. It’s a
pleasure to have
a neat little built-up private stop with
sturdy steps for passengers to board.
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S08 – A face-painted young lassie
looks pensive as she orientates herself in the train after boarding.
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S06 – Shaky and ‘Die Ou Buffels*’ ham
it up in the crew car. Sometimes you find people that are naturally funny
just by having a pulse, and Tony King (Left) and Piet Steenkamp (Right) both
fit square in that category.
* The old African Buffalo
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Pictures from around the shed :
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M01 – Head Cases. A stack of brand
new gleaming white hard hats wait on the club house cupboards. These have
been individually allocated to the regular workshop Steam Team, as a newly
mandated compulsory item of protective gear. We have also purchased hard
hats for visitors to wear.
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M02 – There’s something green growing
in the sun baked gravel of the workshop yard, even if it is stunted and
covered in spines. Any foliage that manages to survive in the Martian
landscape at the Reefsteamers workshops earns my respect!
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M03 – This is Class 15F No.3046 which
was rebuilt from the frames up and even had the boiler demounted. This
engine was the first one worked on by Reefsteamers but was never finished.
She’s literally as new and just needs pipes and brass work to run again.
This is one of the engines for which we seek sponsorship to restore for
Steam in Action.
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M04 – A light snack. James ‘Poopies’
Thomson is the champion eater amongst the Reefsteamers, something akin to
firing a GL Garratt with tomato boxes and toilet rolls. Here, he is contentedly
working through the first box of his five course lunch.
(Picture posed.)
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M05 – A candidate for the
steam-powered Darwin Awards, ‘’Smudge’ Ackerman tests the efficiency of his
new hard hat by using his own cranium. No extra brainium damage was
noticed after the test. That’s the No.93 Booth Rodley steam crane in the
background.
(Picture not posed.)
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M06 – A young enthusiast enjoys a
coach step-ride at the end of his first day out with the Reefsteamers. I
hoped he would remember to pull himself in as the coach passes through the
Western Gates.
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M07 – The joys of trying to energize
your machinery from a rickety and mostly unlabeled distribution board. Andrew
tried to fire up the Punch but was unsuccessful.
The increasingly unreliable electrical and plumbing systems of the old
Steam Depot are items for which we will eventually seek Steam in Action
sponsorship or assistance to repair.
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M08 – The Buffels two-step. While step-riding
during the Saturday Evening shunt, Piet Steenkamp is actually using his
left foot to hold a brake hose down against a dummy to maintain the vacuum
in the brake lines. Normally the hoses are clipped on and then the vacuum line
seals itself – but the clamps for this hose were distorted.
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M09 – The ash pits of the receiving track
steam in the cool of Sunday morning as the locomotive moves off to be
topped up at the coal dock, prior to the day’s trip.
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End Piece :
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EP01 – What a great way to end the day
– a balmy
summer’s evening of shunting with a beautiful engine.
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- Lee Gates -
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