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Reefsteamers Depot News Report
- 26 July 2008 + 2 August 2008-
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Introduction :
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Work continues on the Class 12AR No.1535
‘Susan’ with the addition of two more boiler tubes being found to have
thinned out and needing removal. The lil’ green critter, aka, the 150HP
Hunslet Taylor Shunter was also one of the spanner stars for the day, with
both the locomotive and the spread out bits being worked on.
We had a reasonable turn out of
Reefsteamers, remarkable for a day when we had a train out on the high irons.
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PROJECT – Hunslet Taylor Gear Box Assembly : (2 August)
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My gearboxes don’t leak!
Andrew King
Some work has started on getting the cog-box
back together again for the Hunslet Taylor shunter. So while Mister Berry &
Son were working on removing the engine hood and door braces, and
disconnecting the four engine mountings, to clear the engine for removal, the
gearbox reassembly project was on the go. Unfortunately, the day’s project
ended up stymied with a binding jack shaft gear and a grumpy Chief Engineer.
(Well, grumpier than usual, anyway.)
The jack shaft assembly had arrived in
state at mid-day two weeks ago from Surtees Engineering Works. Andrew had
taken half the depot day off to fetch the shaft. The newly fabricated jack
shaft gear had been pressed onto the shaft, the bearings replaced with a
brand new set with self adjusting barrel rollers, the counter weights had
been pressed and keyed back on and the drive rod pins had been polished. To
get the shaft off-loaded, the bakkie (Pickup) had to be reversed into the
workshop ramp, bouncing over a set of wooden sleepers and hanging four on a 30
degree slope under the overhead walkway. This was, of course, to be able to suspend
a block and tackle from the walkway‘s structure to get the load off the
vehicle. We could have man-handled the shaft off the vehicle with enough
people, slings and cross bars – but as solid and as indestructible as the
shaft assembly looks, a single drop would damage that new gear.
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J01 – An exercise in balancing on the slings, the shunter’s
overhauled jackshaft hangs suspended under the pedestrian bridge, the
shadow of which is visible. Those tied up cloth wrappings at either end are
to protect the new (ungreased) bearings
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J02 – A-brakes … ‘A’ for ‘Andreas’,
who’s applying maximum braking effort
as the heavy load settles on the trolley .
You can see the relative slope of the
ramp by the level ground at the top
of the retaining wall to the right.
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J03 – The counterweight that skewed the works and tried
to roll the shaft off the trolley
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The hoist gang got the asymmetrical load
reasonably balanced on the third attempt (Pic J01 above) – that asymmetrically
positioned drive gear inconveniently adding a lot of weight to one end of the
load. Andrew got the bakkie out from under the dangling load on the second
attempt – literally using sleepers as stepping stones. My respect for Isuzu
went up a few notches. And I’ll never lend my cute little city car to any of
these people! There’s a story that’s been doing the rounds; of a rented
Toyota Tazz that did 140kph all the way from Jo’berg to Port Elizabeth with literally
half a ton of steam locomotive spares on board! **Cough** Maurer! **Cough!**
While the Chief Engineer was doing a stint
of rubber-tired bronco busting, and Aiden McCarthy n’ me standing well clear
and up-slope from this ominously dangling load, the nose-pivoted trolley was
made ready. Andreas Mathee did the honours and threw out everything he
personally had in anchors to hold the load on the slope while the heavy load
came down onto the load deck. (Pic J02 above)
These trolleys can sometimes be difficult
to control as you have to hold the pivoted handle downwards as well as brake
the load. If the handle slips upwards, you stand to lose a few teeth. The
beautiful newly cut gear was protected with a fresh soft knotty pine palette,
with one counter weight lying very conveniently in a slot left by a missing
deck plank on the trolley. Andrew and Aiden (especially Aiden) acted as drag
anchors to get this lot down the slope. The jack shaft tried to roll off
sideways at the lower end as the opposite counter weight, at 90 degrees,
flirted with gravity and its weight pulled the shaft around. (Pic J03
above) Three fellows struggled to control the trolley, act as drogue anchors
and turn the shaft into a safe position, all at the same time – but they
managed. They trundled the shaft into the assembly shop with no chipped gear
teeth and no fresh dents on the concrete slab.
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J04 – Johann (Right) and Mark Berry (Left) occupy
themselves with shifting big chunks
of steel layer-cake. They were very careful
of the flanged sealing faces as this gearbox uses metal-to-metal seals with
no gaskets.
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J05 – Here’s the 450kg capacity column
hoist that is going to see much service
over the next few weeks! It swivels at the i-beam column. You can see
that the crawler
and the tackle is at full reach.
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J06 – Cleanin’ and scrapin’ It wouldn’t do
to have bits n’ metal shavings floating around
in the oil. Johann is swabbing out the sump
while Andrew is carefully scraping the joint
flange. Luckily this isn’t soft aluminium!
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This week’s re-assembly work (2nd
August) started with the clearing up of the assembly area. (pic J04 above)
This diesel locomotive’s gearbox is built like a cast iron layer cake, with
the frame built from four stacked sections. That makes for a lot of heavy
parts lying around from where the outer bearing race spacers were being
confirmed for fit in the newly oversize-machined shaft apertures. Johann
Breydenbach and Mark Berry did the initial clean up (Pic J04 below) using the
450kg column hoist. (Pic J05 above) The crawler beam was almost to the end of
its run and that beam was quivering under the weight. (But still within
capacity) Great care was taken with slings and where we were standing.
The rail trestles were brought out (last
used under the Steam Crane’s Boiler) and with no further ado, the sump pan of
the gearbox was hoisted out and laid flat. Mark Berry ended up back on
working on stripping the engine hood and door supports on the Hunslet Shunter
itself, while Andrew King joined Johann Breydenbach and they got stuck in. The
oil pan was carefully cleaned out on all the inside surfaces and the sealing
surfaces scraped down and degreased. (Pic J06 above) What looks like a depressed
sump-oil reservoir (left of pic) is actually primarily a recess in which the
large jackshaft gear runs.
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J07 – Flossing is good for gear teeth,
as well as our own dental gear.
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J08 – Test alignment of the new shaft.
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J09 – There’s nothing like the silky, heavy
movement of an outer bearing race of a self
aligning bearing – precision engineering.
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The jackshaft was then carefully slung up
and hoisted several times until it would lay reasonably horizontal – no mean
feat with such a heavy gear offset 2/3 along the shaft. Johann took the
opportunity to clean up the gear teeth with the shaft blocked up at knee
height. (Pic J07 above) Then Andrew did something that looked a little odd
– he lined up the shaft exactly over the bearing runs and then swung it away
again. (Pic J08 above)
When he swung the suspended load out the
way, he was careful not to move the chain tackle along the crawler beam –
relying wholly on the radial swing of the hoist to clear the shaft. We’d be
using LockTite to help bind the outer bearing races. But after application
and smear session, it would be important to get the shaft bedded into the
frame as quickly as possible before the LockTite dried and cured. With this
method, it would be much quicker to line up the heavy dangling shaft simply
by swinging the radial arm of the hoist and not having to adjust the crawler
as well. The gift-bearings were then unwrapped from their cloth wrappings and
checked for cracks and deformations, and basically just played with. These
are self aligning roller bearings and are able to run with the outer races slightly
tilted. Because this shaft drives a pair of cranks, the reaction against the
train’s load will act at a point that constantly rotates around the bearing,
90 degrees to the crank. These bearings will be able to constantly re-set
their alignment, and that of the shaft, with the shifting, rotating reaction
from the load.
With the bearings played with, and a final
wipe of the bearing shells, the LockTite came out and was rubbed into those
saddles but definitely NOT licked off the fingers. (Pic B10 below) With
that the shaft could be gently lowered into place and the bearings seated
home. (Pic B11 below) The bearings were gently nudged inwards with a short,
clean tommy bar levered against the counterweights.
A problem arose because one end appeared
to have too big a gap, and the seal cover wouldn’t be able to be screwed home
against the protruding bearing. (Pic B12 below) Andrew wasn’t at all happy
and probably quelling feelings of internal panic as he inspected the shaft
and the bearings on both sides. According to the visible marks on the shaft
though, the bearings had been pressed into the correct locations. It turned
out that the entire shaft was originally built with the bearings slightly too
far apart and it had settled in slightly offset along the longitudinal axis.
There was nothing for it but to hoist the shaft out again – from the half dry
LockTite, which had already established quite an impressive grip on those
outer races. On the second alignment, both bearings were seated with
sufficient clearance to be able to bolt their circular end covers in place.
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B10 – The LockTite is being generously
applied. Just inside the bearing saddle,
the serpentine oil grooves can be clearly seen.
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B11 – Looking like a cross sectional view,
the shaft and its bearing has been seated.
The circular seal cover can just be seen
lying against the counterweight.
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B12 – Lee points at a telltale overly wide
gap between the bearing and the
saddle face. The seal cover has been
snugged up to test whether it could
be screwed all the way home.
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With the shaft in place and freely
spinning, Lee was tasked with priming those new bearings with an oil can to get
some oil on those rollers and spread around inside the races. (These weren’t
pre-packed bearings.) A beautiful fine-nozzled antique valve-equipped oil
can, courtesy of Patrick Ackerman, did the trick. (Pic B13 below) We fed
oil onto the bearings with Andrew gently turning the heavy jack shaft over. I
even filled up the oil can before handing it back – scavenging for MH oil from
mainly empty loco oil cans seeing that the oil drum was empty.
The second frame was then hoisted (Pic J14
below) and set up in an upside down position upon wooden blocks on the
floor. We scraped off the bare-metal sealing surfaces, (Pic J15 below) with
some fine filing on the seriously crusty bits, before watching King do the
cake decorating act with a tube of silicone sealer. The caulkin gun appears
to have disappeared, so Andrew simply pushed an adjustable spanner into the
cartridge with the head pressing into his tummy. He then pulled the
cartridge back against his own stomach muscles (Behind his belt buckle) to
extrude the silicone bead … talk about macho tummy crunches. As I’ve said
before, this little grey haired fella is a tough old rivet.
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J13 – Priming the dry bearings with fresh
MH oil, right through a pilot hole
between the two inner cages.
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J14 – Hoisting the 2nd frame. A bearing
for the transfer shaft, which carries a bevel
wheel to turn the drive 90 degrees, is
visible through the gear wheel aperture,
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J15 – Scraping for glory. Because the
frame joints span at the shafts, gaskets
cannot be used. The surfaces have to
be perfectly clean and degreased to be
sealed with a compound.
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I made some comments about potential oil
seepage, aka, automatic built in locomotive frame rust proofing protection, which
was the source of the quote at the start of this section!
The center portion of the frame, the base
frame, went onto the sump pan with little trouble but naturally needed some
alignment. (Pic J16 below) This is the section of the gearbox frame that
actually bolts into the locomotive’s frame plates. Luckily the still semi-liquid
silicone sealer provided some impromptu lubrication, and it was easy to line
this heavy section up using the massive bolts through the jackshaft bearing
cradles and the matching bearing caps.
A nasty surprise ensued because the
previously freely moving jackshaft had locked up tighter than a politician’s
purse. That’s always bad news as it usually indicates that a bearing has
been crushed somewhere. However, in this case, it turns out that the main
gear for the jackshaft was slightly out of place. It protrudes through a
built in tooth guard into the base frame and was actually binding right up
against the frame’s side wall. (Pic J17 below) Very disappointing and
maddening.
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J16 – The base frame has landed. Notice that the cross
piece has no ears for bolts – the bearing that sits in that saddle relies
entirely on the strength of the material to grip
and stop the outer race from spinning – a
definite weakness in the original engineering.
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J17 – The jackshaft gear was jammed
right up against the frame plate. You can
see the large gap on the right hand side.
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J18 – If you look carefully, you’ll see that there’s
evidence of contact between the gear wheel and the frame – this problem had
also occurred some time else in the locomotive’s life and was probably
‘repaired’ when all the bearings were shimmed up with brass stock.
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In similar fashion to the bearing displacement
issue, the shaft was checked again and it turns out that the gear is properly
located on its original marks. But it always was slightly offset. (Pic J18
above) It turns out that the shaft and gear placements weren’t measured against
the counterweights when the gearbox was dismantled by the day staff, and when
Surtees used their 400 ton press to get the gear back on, and using the
original marks for alignment, they innocently replicated the mistake. The gear
needs to be moved about 6mm but we don’t have the equipment to do this. So
the entire shaft has to go back to Surtees Engineering for a another game of
400 ton patty-cake
Thus, a grumbling and slightly despondent Andrew
King had the delightful task of dismantling the day’s work. He’s been
itching for three weeks to get the job done only to have this set-back.
Dismantling included the extra chores of cleaning
the half-cured silicone off the mating surfaces and scraping the remains of
the LockTite from the bearing saddles. So it was a disappointing end to an
afternoon’s work – but a potentially serious problem was found before gearbox
assembly continued much further. Imagine the waste of time and damage if the
gear was found to be displaced after the gearbox had been assembled or even
reinstalled between the loco frames.
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PROJECT : Hunslet Taylor Hood removal :
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The lil’ green critter is to have the
entire engine removed. The suspected dirty oil galleries need to be cleaned
out and of course, all the bearings and seals inspected. The three pistons already
exposed by the withdrawal of the rear engine block are to be treated to a new
set of piston rings. This being a diesel, a compression ignition engine, the
condition of the piston rings is quite critical. However, only replacing the
piston rings on the rear three of the six cylinders will result in the rear half
the crankshaft being subjected to higher compression and higher combustion
pressure from cylinders that are running more efficiently. This would impose
a torsional stress on the crankshaft at the center bearing and lead to failure
down the line.
The engine cannot be withdrawn through the
frames and neither can it be moved sideways. It has to be hoisted upwards.
Thus, the green engine hood had to be removed. Although the engine cowling
and hood assembly may resemble that of an oversized old fashioned truck, the
hood doesn’t hinge. It is bolted and bolted and bolted and bolted and bolted
in place with several dozen rather crusty bolts. The hood was removed three
weeks ago at the end of a quiet Saturday and was quite an aggravating job.
The basic game plan was to fire up the battered but useful LPG-powered Hyster
forklift, bring it in perpendicular to the hood (Pic H01 below), and couple
the tines to the central lifting-eye. (Just in front of the shunter’s bell.).
(Pic H02 below)
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H01 – Close quarters game plan,
using the forklift with wheels at full
lock to hoist the engine hood.
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H02 – The sling and the bell, probably
not a bad name for ye olde English Poob.
That bell pealed a few times when the
hood finally unstuck! The bell cable had
already been disconnected in this photo.
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H03 – The retracted exhaust silencer and
the integral stack, with the classic clapper flap on the top. Mercifully,
this and the bell cord were the only items that had to be removed.
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Getting the bolts off the hood was an
exercise in contortionism. This simple little engine cover is massively over
engineered – it’s almost as if Hunslet thought it might fly off over the cab at
the blinding fast shunting speed of 15kph. As is becoming usual with this
particular locomotive, the bolts were of odd sizes and most of them quite
awkward to get at. The side brace bolts were easy enough, albeit with
restricted swing on the spanners. The rear bolts on the scuttle are hidden
behind the diesel fuel tank, while the front bolts are nestled deeply in
around the radiator and the fan cowling. The exhaust stack’s upper bracket
was removed and the stack pulled downwards into the engine bay. (Pic H03
above) Odd enough, although exhaust bolts on any vehicle are usually rusted
and seized, these ones unscrewed by hand tools only. Although the exhaust
stack stands in line with the front three cylinders, which are still bolted
down and intact, both the exhaust and induction manifolds are full length
six-way units. So the entire engine was innocent of manifolds, even though only
the back three cylinders had been dismantled, and the exhaust stack was able
to conveniently slide most of the way down into the manifold space. You can
see it in the retracted position in Pic H06 below.)
The vertical brace bolts along the hood
were fairly simple. The scuttle plate bolts were more awkward needing an
individual in the cab to hold the heads. The bolts in the rear corners,
though, were seized and had to be cut out. (Pic H04 below) The faded forest
green paintwork is now scorched and has burn streaks on it – but the shunter
is to be completely repainted anyway. The front bolts were seized as well
and it was a weird sight to see the smoke wafting up through the riveted
seems as the torch work was going on within. The front bolts were badly
obscured by the radiator’s header tank and no bolts could be found in the center
line – which seemed odd and basically just too good to be true.
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H04 – Torching off the rusty rear corner
bolts and scorching the paintwork in the
process. We had to watch the fire risk as
the rectangular box visible behind Shaun’s scapulae is the diesel fuel
tank.
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H05 – A view at the right rear corner shows
the tightly spaced bolt holes and a design
problem. The rear of the hood is braced with
a vertical plate and water can obviously
penetrate between that and the cab scuttle
– leaving the rust that you can see here.
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H06 – Hanging on stubbornly, the
engine hood has sprung uncoupled
at the rear but it’s obviously still
attached at the front somewhere. Notice
the two vertical braces – these were
removed by Berry & Son two weeks later.
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The first attempt at lifting the hood with
the forklift tines was a failure. The forklift itself just about stalled
trying to drive its own load-locked hydraulics, and the over-sized front
tires visibly depressed as the poor little Hyster was basically trying to
lift the entire locomotive. Hunslet - 1. Hyster - 0. Interesting that the manky
old hood bolts withstood the traction. The missed bolts were undone and on
the second attempt, the tension was unbearable. The rust holding the rear
end of the hood sheared (Pic H05 above) and it suddenly let loose and came up
with quite a loud bang and a vicious jerk. (Pic H06 above) Luckily the
rounded front of the hood wasn’t distorted. We were also lucky not to smash
the glass panes of the windscreen. Although they are to be replaced, we’d
rather not have scattered glass fragments decorating the workshop bays, thank
you very much.
With the engine hood sprung at the rear
end, the front end looked ominously like the radiator would have to be
removed, along with its necessarily large thermo-siphon top-tank and the deep
fan cowling. But that doesn’t really make sense to have to dismantle engine
opponents to remove the hood. Even Hunslet wouldn’t build a locomotive that
badly! Because of the tight clearances at the front end, we were working
blind. Technology came to our aid – my digital camera (both of them
actually) has a pivoting and tilting LCD feedback display. We set the LCD
screen at 90 degrees ands used the camera optics to look around 90 degrees, right
into the tight space in front of the header tank, with a torch shining up
alongside the radiator. The extra bolts were found – higher than expended
and it turns out that the bolts that hold the ‘Hunslet’ script nose-badge
also hold the hood down at the front end. Naturally, they were dreadfully
rusty – 56 years of rain water running down between the hood’s front bevel
and the cast iron badge would have that effect.
Andrew ‘Noddy’ King did the torching,
being very careful not to damage the precious cast iron Hunslet badge. (Pic
H07 below.) That badge, behind the weathered, peeled paint, and the fresh
scorch marks, is a beautiful casting and it was being looked at with envious
eyes for wall décor! Dr. ‘Smudge’ Ackerman, himself a collector of railway
themed badges and name plates, jokingly laid down the line. But maybe we can
make a replica of this name plate...
Because the bolts could only be cut flush
with the badge and not the hood, the cut off bolts would obstruct the hood
from being lifted. So the hood had to be wriggled and walked forward on the
vertical braces to help break the rust bond and to clear the protruding
bolts. The hood came off literally with a pop and it swiveled upwards at the
front end without knocking anyone’s teeth out. (Pic H09 below) You can
clearly see the rusty front plate that is normally inaccessible behind the
radiator header tank.
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H07 – Andrew King – Scrap Merchant.
He’s delicately cutting out four rusty
bolts without damaging the nameplate
in which they are embedded.
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H08 – The removed ‘Hunslet’ badge with
scorched paint but undamaged engraving.
The green plate behind it is one of the engine
side covers leaning against the GMAM Garratt
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H09 – Hooray … and up she rises.
Hooray … and up she rises,
Hooray and up she rises-es,
…early in the evening!
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The suspended load was a bit tricky to get
out as the forklift had to be reversed at full steering lock. The dismantled
components had been thoughtlessly put in the turning arc so there was a mad
scramble to get everything out of the way. (Pic H10 below) The GMAM Garratt
No.4079 ‘Lyndie Lou’ got a gentle flank-on love-tap, but we avoided putting
the hood through the cab windows and the wind deflectors. It took three
Reefsteamers and a forklift to walk the hood out and to put it safely out of
the way in the open workshop yard. (Pic H11 below)
What a palaver!
The next time you have to open your car’s
hood (or bonnet), appreciate the fact that all you have to do is pull the
release, uncouple the safety latch at the front end and swing it up on
HINGES. What a luxury!
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H10 – K53 has nothing on the Reefsteamers.
Here is how to reverse at full lock in narrow
confines and handling a penduluming load.
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H11 – The hood finally kisses the
concrete in defeat. Notice that the
coaching crew (Coenie and Fred) have
joined us after finishing their day’s work.
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H12 – A typical unpadded
Hunslet engine mounting!
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The hood saga continued last week (2nd
August) with Mark Berry and his son, Ryan, being tasked to remove the side
braces, the diesel fuel tank and to uncouple the engine mountings. It was a
simple sounding job complicated by bolts deeply recessed between flange webs
and the now expected Hunslet assortment of odd bolt sizes. They tackled the
engine mountings first. The engine is mounted on four pads, one at each
corner and each with two bolts. There are no rubber cushions. (Pic H12
above)
It’s always great to see a father and son
work together. Ryan ended up working from the walkways (Pic H12 below) being
smaller and more agile than his dad – who provided the torque and the
technical expertise. Because they worked on uncoupled the engine mountings
first (as higher priority) the four vertical supports restricted the swing of
the tommy bars. (Pic H14 below) The deck was completely cleared by the end
of the day with the four vertical braces being removed and the diesel tank
being nothing more than an empty space. The last two remaining control rods
had been removed (for the injector pump) Apart from the radiator cowling
and the hoses, and the starter motor\battery cables needing to be bundled up
this engine is ready to be lifted for strip down and a good old fashioned
Reefsteamers quality overhaul.
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H13 – Ryan Berry makes a usefully
compact package as he folds up his slender
form to get into the corner of the engine bay.
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H14 – Mark Berry applies some grunt to
the rear engine mountings, as his son,
Ryan, approaches with extra sockets for
the odd sized nuts. By steam locomotive
terms, this is minimal leverage!
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H15 – A hood brace being removed.
The deeply inset oddly sized bolts were
quite troublesome. The diesel fuel
tank has already been removed.
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PROJECT : Diesel Shunter crown wheel gear stripping.
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G00 – There is beauty to be found in engineering. Here
the Hunslet’s
crown wheel shines like burnished gold in the morning sun shine.
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Yeah, more Hunslet work.
This job is interesting to note as it
shows how we Reefsteamers are not shy to IMPROVE the original engineering and
design of our locomotives and rolling stock. In this case, we are fixing up
a poorly done modification as well. The Vesconite™ bearing retrofit program
is an ongoing example, but here is an interesting case of modifying original poor
design in a 56 year old diesel locomotive gearbox. (Pic G01 below)
Back in May, during the evisceration of
the gearbox’s giblets, the crown wheel and dog clutch set wouldn’t come apart
– even after being locked in a pipe vice and heated to try to break the grip
through thermal expansion. (Pic G02 below) This locomotive’s gearbox has
been modified over the years and the original reverse gear and friction
clutch has long since been removed. In the current drive train, the reverse
gear set comes first (incorporated into the retro-fit torque converter), a
short universal jointed drive shaft and then a set of original high and low
speed gears. There was a clutch and a reverse gear train up on the crown
wheel shaft. However, on this particular locomotive, the forward gear crown
wheel gear has been locked permanently to its shaft via its dog clutch, the
second beveled crown wheel omitted altogether and the extra gear linkages removed,
making this gearbox a two speed single direction unit. The reverse gear is provided
(at 1:1 ratio) by the torque converter bolted directly to the engine.
You can see the locked bevel gear in situ
in Pic G01 below. Notice that the dog clutch is permanently engaged and the
other side of the dog clutch, as modified, never engages anything. Those odd
looking braces occupy the space where a second bevel gear would have been for
reversing. The retro-fitted ‘braces’ are actually oil channels designed to pick
up oil dripping down the crown wheel and channel it through to the bearing at
the outer end of the shaft. This shaft, which would normally be a secondary
main shaft after the 2-range gear set, is now simply used as an intermediate
shaft.
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G01 – The locked crown wheel in situ. (10 May 2008) The
small bevel pinion on the
right is the primary drive coming in from
the 2-range gear set. The small
pinion at the bottom of the photo engages
with the big jackshaft gear. The
intermediate, or crown wheel shaft
is actually made in two halves.
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G02 – (18 May 2008) Still smelling of hot steel and
cooked oil, half the intermediate shaft on the pipe vice in an unsuccessful
acetylene torch-aided attempt to disengage the locked dog clutch. (Around which
the chain is looped.) Notice the threaded peg that engages in the other
half of the shaft.
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G03 – (18 May 2008) I’m pointing at a
totally unnecessary roller bearing that
never spins in post-modification service.
The splines in the foreground are for
the jackshaft drive pinion.
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This is a constant mesh gearbox, the same
basic principle as used for motor car gearboxes except it doesn’t have the
refinement of synchromesh and baulk rings of course. In a constant mesh
gearbox, the various selectable gears that are used to transmit the power are
actually mounted on their shafts with bearings, and can spin freely on the
shaft like a doughnut spinning on a broomstick. But they cannot move
longitudinally. The dog clutch, is splined to the shaft and thus does not
rotate freely – but it can slide up and down longitudinally. When the dog
clutch is shifted along the shaft by the selector fork, the axial teeth of
the dog clutch engage the matching internal axial teeth on the gear. The free
running gear is thus now locked to the shaft by means of the dog clutch’s
splines and can now transmit torque. The other, unused gears remain engaged at
their gear teeth (hence the term ‘Constant Mesh’) but they rotate at different
speeds AROUND the shaft and not with it. In a modern car gearbox, when
you’re in top gear, the 1st-4th gears are all still
driven by the engine and are revolving simultaneously at different speed around
the main shaft while only one gear at a time is locked to the shaft and
transmitting power. The colloquial term ‘gear shift’ is actually incorrect
and should be ‘gear selector.’ It is actually impossible to grate the
forward gears of a car (or this locomotive) as they are always engaged. It
is the clashing teeth of the dog clutches that make that grinding sound.
(The only gear that is physically shifted is the reverse gear pinion.)
In the modified Hunslet loco gearbox, that
permanently engaged bevel gear and dog-clutch combination was left with the
roller bearing that would normally allow it to revolve freely around the
shaft when the other bevel gear would be selected in a two speed version of
this gearbox. (Pic G03 above) That ball bearing, although it hasn’t been
rotating between the gear and the haft, has become worn and the stationary hardened
rollers have indented the bearing races over the years. This is allowing the
locked bevel gear to tilt on its shaft, with the torque reaction. An
engineering principle is that a set of gears (and their shafts) always try to
move apart under torque reaction. The displacement in the shafts (or the
bevel in this case) upsets the mesh pattern of the gear teeth. This gearbox
has been cut with involuted teeth of which their profiles maintain a point of
contact at a constant radius from the shaft centerline as the teeth rotate in
and out of mesh. Spread shafts (or a tilted gear) results in a pulsating
drive and the stress moving to the thinner, weaker parts of the teeth and
premature disengagement of mesh of the individual gear teeth. The result is
the teeth start to chip and round off, the damaged teeth damage other gear
teeth and you eventually end up with a stripped gear.
Although the crown wheel is still in reasonably
good shape (Pic G00 far above), it would be false economy to reassemble the
gearbox with those worn bearings, only to have the crown wheel damaged a year
or two down the line. The actual work started with the cleaning of the gear
and removal of the roller bearings themselves. They were, naturally destroyed
in the process and left their indented outer races within the gear’s core.
The project is to re-assemble the intermediate shaft with the locked crown
wheel supported on a nice solid bush the exact size of the unused roller
bearings.
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G04 – Lee points at one of the indented
outer bearing races to be removed. You
can see two of the three initial notches cut
into the spacer. It’s odd to think that those
axial dog teeth are still in unused factory
condition after 56 years of service.
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G05 – A goggle-eyed alien heats up the spacer
rings while dodging the sputtering flames of
the igniting residual oil film. Notice that
Johann is holding a box of matches – the flint striker for the acetylene torch
set seems to have gone missing.
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G06 – Success! The spacer has broken into
two halves. Note the correct safe use of a
copper hammer for close-quarter chisel work.
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Andrew King and Johann Breydenbach did the
strip down. The project proper started with removal of the spacer rings that
ran outside of the bearing races. A cold chisel was used to make three
notches 120 degrees apart in the spacer. (Pic G04 above) Then the
acetylene torch was applied to destroy the tempering of the steel of the
spacer rings (Pic G05 above) – with deeper, localized heat penetration at the
notches. This facilitated further chiseling – with Johann holding onto that bucking
gear for dear life, and the spacer ring eventually came out in two pieces. (Pic
G06 above) It took much prying and whacking to break through the spacer and
then to bend the halves inwards, as the ring of dog teeth prevented the drift
from being tilted inwards.
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G07 – The indented outer ball-bearing
race came out intact. The whole process
had to be repeated for the other roller bearing and its spacer at the blank
side of the crown wheel.
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G08 – Johann is scraping the spacer clean. All that
muck that you can see had managed to work its way in from the gearbox oil,
through the bearing ball races and into the tiny radial clearance space deep
within the crown wheel. Imagine what that dirt did in the cavities within
the functioning ball bearings over the years….
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G09 – An identical scrap ball bearing and
a stock blank that is to be turned down
to a bush to replace the unused roller
bearings within the crown wheel.
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The spacer ring was difficult to get out
because the diameter was wider than that of the inward pointing dog teeth.
But the bearing races are of smaller diameter (otherwise you couldn’t fit the
bearings in the first place.) Getting them out was a matter of ‘springing’
the grip and then tapping them out from the other side. The lipped outer
race (Pic G07 above) was quite convenient as a drifting point. The
intercostal spacer, freed up by the removal of one bearing race, could now be
slipped loose. (Pic G08 above) This component, originally used to hold the
outer bearing races apart, it to be re-used to hold the new blank bushes
apart.
James has already started selecting and
cutting down cylindrical stock to make two blank bushes to support the crown
wheel. (Pic G09 above) He’s basically making dummy bearings and those
bushes should last forever. Internal diameter is 95.25mm and the other is
171.46 and the thickness is to be 28.6. The bushes are to be machined to a
tolerance of 0.02mm! But hat is an accuracy of work that comes naturally to
our senior machinist, James Thomson. You can see the start of the process in
Pic G10 below, using the lathe’s tailstock to start drilling the center hole
for the shaft.
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G10 – The start of fabricating a bush as a dummy
bearing. This is a high speed
shot – the lathe is running in this picture.
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PROJECT – 12AR Boiler tubes ;
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B00 – A firebox aglow with a different sort of light.
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Let’s see how thin the boiler tube is…
Patrick Ackerman
The boiler tubes for the Class 12AR
No.1535 have been replaced, including an extra two that were found to have
thinned out at the Smokebox end. What is interesting about this job is that
none of the men who did the work are over the age of 30.
For a detailed description of the boiler
tube operation, you need to read the last issue of the depot report. I’m NOT
writing all that lot again! :o)
We lost a day’s schedule on the job as
Shaun and Lee were to expand and fit the new tubes on a Sunday.
Unfortunately, the right sized expander had been locked away and we couldn’t
track down the keys. However, the delay was made up for the following
weekend with two half expanded tubes being fully expanded and 4 new tubes
being fitted from scratch.
All the expanders were available today.
(Pic B01 below) A range of four expanders and four mandrels were used. As
the various sized mandrels are all interchangeable with the expanders, This gives
the operator 16 combinations. Dawie and Patrick saved time using pneumatic
assistance to both expand the copper pipe from which the ferrules would be
made and later to expand the tubes within the tube plate. You can see the
very low-geared pneumatic motor in use in Pic B02 (Below) The boiler boyz
used the 7 ton Dean Smith lathe once more as a pipe vice.
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B01 – Two tube expanders and three
tapered mandrels. The tilt of the tapered
roller is seen clearly on the right unit – which
is what screws the unit in. The taper on the mandrels matches that of the
rollers.
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B02 – Pneumatic motor in use. Patrick (Left) holds the
reaction lever. Dawie (Right) is actually controlling the direction of the
motor by rotating the hand grip’s sleeve.
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B03 – The copper tube, from which the
tube plate ferrules will be made, has visibly
expanded. The motor has just been
reversed and you can see the mandrel
just starting to back out.
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The operation went much quicker with
pneumatic power (Pic B03 below) even though the motor isn’t running
optimally. Because of the increased rate of work, special care was made to
keep the copper annealed – it told at the end of the day when the oxygen gas
bottle prematurely ran dry!
In the smoke box, the two tubes that had
been already fitted were not expanded at the smokebox end – as they protruded
a little too far. So the protruded ends were carefully ground down straight
and even with the existing tubes. (Pic b04 below)
Andreas Mathee came walking in for his Depot
Day and he joined the boiler team ... and wouldn’t be clean again for the
next 7 hours! The youngsters got going with expanding the copper ferrules
and cutting fresh tubes at the same time. With the pneumatic ,machinery,
expanding the remaining 5 ferrules (Pic B05 below) was quite easy – although
the firebox stank of oily exhaust air. It filmed up my camera lenses too, so
I had to get out of there and clean up my optical gear.
Patrick Ackerman had brought in ‘The Bread
Slicer’ for speedier cutting of the other tubes. (Pic B06 below) Although
the could only be annealed at one end at a time (pic B07 below), ‘cuz we only
have one acetylene torch, the dressing, descaling and polishing of the tube
ends could be done at both ends simultaneously, which speeded up operations.
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B04 – Short back and ends please. An overly
long boiler tube is ground back. The small
open hole to the right of the spark-filled tube
is the threaded aperture for a washout plug.
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B05 – All the copper ferrules have been
expanded into place and a fresh cut tube
has just been slipped through the tube plate.
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B06 – ‘The bread slicer’ makes short,
straight work of cutting the fresh tubes. .
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With plenty of sandpaper strips being on
hand, the polishing went well. (Pic B08 below) The tubes went into the
boiler with little incident. (Pic B09 below) Even author Paul Hloben, when
he came in the afternoon, has a go at feeding a tube in. The air motor came
in useful to snug up the tube at both ends. But the final expansion had to
be done by hand as the motor had insufficient torque to complete the job to
satisfaction.
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B07 – Better look carefully before
picking these tubes up! So far as I know,
no-body’s skin has been incorporated
into the locomotive boiler
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B08 – Andreas takes a turn at polishing drill – yank a
strip of glass paper back and forth to clean off the burnt remnants and
scale.
He’s wearing his dad’s hard hat – a Reefsteamers form of growing up to fill
someone’s shoes..
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B09 – Andreas (Left) and Dawie guide a new boiler tube
in while Patrick, within the firebox, waits to guide the end through the
tube plate.
We want to pass the skills of steam to a younger
generation – which certainly bearing fruit with the oldest of these guys
being 28 years old and busy re-tubing a loco boiler
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I wasn’t around to take photos of the
smokebox end work being done. But I was around to catch some photos of the
firebox ends of the tubes being expanded. The firebox end is done first.
Andreas was careful to ensure that the tube and the expander were well
oiled. (Pic B10 below ) Then he used a vernier caliper to measure the depth
of the tube’s protrusion – which must be between 8-10mm for effective beading
and welding. (Pic B11 below) An over-length tube can be ground down, but
one that is too short basically means the tube has to be pulled out and
replaced. When the tube was 9mm out – Patrick clamped onto the other end
with a vice grip and a large screwdriver as a tommy bay to stop the tube from
rotating and moving inwards. While one has leeway in fast set up at the
smokebox end, one has to be careful to set things up slowly at the firebox
end before the tube starts to grip within the ferrule. (Pic B12 below)
Applying the air tool prematurely would overwhelm the grip the fellow at the
other end and might push the tube right through into the boiler cavity.
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B10 – Some fresh MH oil for the tube
ends and for the expander itself. Notice that the antique oil can has an
anti-drip valve for the sprout.
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B11 – One of many checks for the
critical minimum depth of the tube –
Andreas Mathee checks that the tube
protrudes 9mm and definetly not less than 8.
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B12 – The expander and the correct
mandrel is set up by hand and a wrench
before applying the pneumatic grunt.
Andreas wipes his oily hands before
setting up the air motor.
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The expansion work, primarily done by
Dawie and later, Andres, went with little trouble. However, the finishing
work had to be done by hand and a heavy ratchet. But because the pneumatic
motor wouldn’t be used for the full expansion work, it could be operated by
one person. (Pic B13 below)
Two of the non-removed tubes had suspect
looking ends, one of them definitely looking a bit ragged form a mixture of
abrasive blast and corrosion. It was quite obvious after some exploratory
tapping during the process of latching onto the other end of tube No.7. (Pic
B14 below) When Andreas finished his expanding and the smokebox end of the
tube was fully seated in, Patrick ground back the ragged tube to check the
thickness of the material.
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B13 – The pneumatic motor in use.
Because the guys realised the motor
wouldn’t finish the expansion job, you
wouldn’t have the torque reaction and the
job had degraded to single man operation.
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B14 – Patrick latches on to hold the tube still while
the expander is working at the other end. Notice the corroded tube just
above the washout plug, 10 o’ clock form the vice grips.
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B15 – Cut down beading and weld form the
firebox side. It’s a nasty job grinding these
down as one has to be careful not to cut into
the tubplate.
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What he saw wasn’t good and he called the
Chief Engineer in for advice. Andrew condemned the tube and so it was to be
withdrawn – just when we thought we’d finished the job! Andreas got to work
with a small angle grinder, to cut away the rolled over bead at the firebox
end. (Pic B15 above) It’s a nasty, noisy job and delicate too as you can’t
cut notches and grooves into the tube plate. Meanwhile Patrick fired up the
torch and worked on cutting groves at the top and the bottom of the tube at
the smokebox end. With grooves cut in, the tube would collapse with the use
of a chisel. Naturally, one mustn’t torch a notch into the tube plate. The
process involved using the sides of the acetylene flame instead of the tip
and center. (Pic B16 below)
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B16 – Acetylene Torch brain surgery –
one slip and the patient dies. s
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B17 – Makes the firebox look luxurious,
Patrick folds himself up behind the table plate
and underneath the superheater risers
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B18 – Removed boiler tube clearly showing
the slots cut to collapse the expanded tube.
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7 tubes were replaced and two more tubes
were withdrawn , so the boiler project isn’t quite done just yet!
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PROJECT : Perimeter fencing project – new gates :
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By Depot-Day, 2nd August, the 5
new gates had been fabricated. Andre van Dyk spent the day welding and
supervising his brand new fencing team. Newly joined Reefsteamers members
Miles Buckton and Richard Marshall were put to work – probably a bit
surprised at it not being locomotive work, but they did the job in good
spirits. Two gates had already been built and by the end of the day, three
more gates had been fabricated from scratch and stacked against the walls.
As usual, the gates are being fabricated
from scrap super heater elements. However, stocks are running a little low
and some conventional scrap piping (from a compressed air line) was used for
cross braces. Cutting of the main frames was done on a semi-mass-production
basis with Miles wrestling the grinder and Andre acting as a highly skilled self-propelled
work-weight. (Pic F01 below) The ends of the tubes were flattened for
welding in the 50 ton press and welding done with an inverter welder. The
vertical sections were left circular but the horizontals and the diagonal
braces all have flattened ends. (Pic F02 below)
Welding is thus along the full length of
the flattened end that buts against the sides of the cylindrical verticals –
these gates are going to be tough! (Pic F03 below) However, these gates
won’t be locomotive proof. But they won’t sag under their own weight – which
is definitely irritating when you have to lift a sagging gate off from the
rail heads to swing it around. It’s even more irritating when a sagging gate
tends to swing closed again, just as you are trying to roll a hundred tons
plus of steamed steel between the gate posts.
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F01 – A bundle of scrap tubes being
cut at one go – Miles Buckton enjoys
his first Reefsteamers project.
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F02 – A fresh super heater element end
just about to be flattened under 50 tons
of hydraulically generated pressure
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F03 – A. lower gate corner, with the
weld still cooling and showing the
wide welding area at the butted joints.
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The gate gang were careful to get the
gates square – using the diagonal measurements to proof and square the gates.
The fact that the other guys didn’t have welding masks slowed the job down a
bit as they had to frequently stop work and face away from the welding arc.
(Pic F04 below) The gate joints and diagonals were seam welded along one
side and then, after confirmation of squareness, the gates were lifted on end
and welded on the opposite side, especially at the braces. (Pic F05 below)
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F04 – Andre left the depot with a good ultra
-violet tan on his knees. Notice the feet of
the other guys, facing the opposite
direction as they didn’t have welding masks.
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F05 – Vertical welding to get both sides of
all the joints tightly buttoned up. Here,
Andre van Dyk is actually finishing up
the welding of the latch frame
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F06 – ‘Pops’ van Dyk cuts up pre-stamped angle iron to
fabricate the latch frames.
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‘Pops’ Frans van Dyk fabricated the three
latch frames from a length of the pre stamped angle iron that were made as
conductor carriers. He was working at the main machine shop vice and
usefully so, for he was also fabricating a seriously delicious chicken curry
and was in close proximity to the kitchen. The latch frames are not of
welded sections. They were slit down a web at 45 degrees and then bent in
the vice. (Pic F07 below)
Miles and Richard had the repetitive job
of mounting the insulators – using 90 of them – 15 per pole. As these poles
weren’t stamped, they marked a master pole with engineering chalk, drilled it
out and then used the poles to transfer measurements. (Pic F08 below) These
poor schnooks, on their first day at the depot, had to drill at least 90
small bore holes in circular section high grade steel. The number of broken
drill bits is off the record. (I didn’t dare ask!)
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F07 – Using a vice as a bending brake,
Frans has just finished this latch frame
and is making fine adjustments.
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F08 – Keep going Mr. Buckton! Seven holes
drilled and 83 more to go! You can see the
chalk markings on this fence frame.
Naturally these fellows took
turns with the drill.
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F09 – An almost completed gate
gleaming (not) on the assembly floor.
Only the bobbin insulators for the
latch frame remain to be fitted.
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The insulators were mounted with cadmium
plated self-threading pins – and were applied with the drill. It would have
been dreadful work tapping the bolt holes by hand. Even so, the drill worked
jolly hard and some of the holes ended up with stripped thread, so fresh
holes has to be made. It’s not the fault of our guys, or the bolts, for that
matter. It’s just that the steel of the tubes is harder and thicker than the
mild steel that you would normally find being used by electric fencing
contractors. The five gates were completed by sundown and stored next to the
grinding station. (Pic f11 below)
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F10 – Two new insulators fitted with
modern self-tapping mounting pins.
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F11 – In-house Fabricated gates wait safely out of the
way for wiring and installation.
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PROJECT : Catering :
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People that love steam engines .will often
put other talents into use apart from the footplate and the mechanical work.
Andre van Dyk is one of these, and he has proven to have a talent for bunk-house
style cooking. He also gets good deals on ‘bosveldt’ foods, particularly the
meats. Andre has, in fact, been cooking lunches for the Reefsteamers over
the last year and a further fact that not many have realized, he has been feeding
the entire club at his own monetary cost.
Thanks, Andre!
After a hard morning’s work, it’s pleasant
to have a hot lunch to look forward to. The arrangements were initially
rather casual, which meant that we often went the whole day on a few
biscuits. This had been discussed and it was determined to properly feed the
depot teams on Saturdays – but that it’s the least the club could do is
provide food for those volunteers who have given freely of their own time.
It was determined then by the board to put a part of the monthly budget
towards lunches and Andre van Dyk has committed to arranging ingredients and
doing the cooking. So we’ll be getting a warm meal every Saturday and
usually a BBQ (Braai) on Sundays. We usually do this on a bring-n’-braai
basis or give Andre 20 bucks or so for the meat n’ bread. Reefsteamers
lunches are usually very social occasions!
For the benefit of overseas readers, a
typical Reefsteamers meal, shown below in CS01, is what we call ‘wors and
sous.’ (‘Wors’ is pronounced ‘v-w-orr-s’) The sausages are what we call
‘Boerewors’, which is a spicy coarse grained ‘farmer’s sausage.’ There are
many inferior knockoffs out there, but good quality Boerewors is hard to
beat. The white stuff is ‘pap’, a stiff maize meal porridge. It is the
staple starch of the African population but popular as a casual meal
ingredient amongst the whites too. In of itself, it can be stodgy stuff with
little flavour. And badly cooked ‘pap’ can be used to seal brake vacuum
lines and smokebox leaks. But its neutral flavour goes well with everything
and it’s great accompanied with gravies or stews. The sous, literally
‘Sauce’ or more correctly, ‘gravy’ is Andre’s specialty – sometimes curry,
sometimes savoury, sometimes sweet n’ spicy, and sometimes
blow-off-the-top-off-your–cranium chilli. This kind of food cooks with
little supervision, so this chef can leave the kitchen to do some work in the
depot while lunch is going! (Pic CS02 below)
It’s worth coming to the depot just for Saturday
lunch!
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CS01 – Typical Reefsteamers lunch – Boerewors, pap and
sous.
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CS02 – The master chef at work. You
see by his clothes that he’s been at
work at the depot too – but as long as
the food is good, we don’t worry if the
chef isn’t dressed in formal whites!
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CS03 – Manual stoking. Don’t forget to put
some in the back corners Mr. King. Ultimate
endorsement – Andrew King having seconds.
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Although we’ve seen a lot of Andre lately,
as he’s the Project Manager for the fencing, his ability to be available on depot
days is a bit cyclic. Andre has a demanding IT job and is one of the few
Reefsteamers with a young, growing family. (Most of us are either single or
widowed.) It’s been frustrating for him, and for us, who need every pair of
capable hands we can get. But with the catering job, he can still be
involved even on days that he has to be at home, or doing IT work. He sometimes
cooks at home and brings the food in at about mid day. So our Mr. van Dyk is
fast becoming one of the most popular men at the Depot over the next few
months.
Actually, Frans van Dyk, Andre’s dad, made
lunch last week – a piquant sweet fresh chicken curry and rice. It was
fantastic and I felt sorry for the 12AR boiler tube boys who took too long to
extract themselves from the loco’s innards and pitched up while nearly everyone
else were nearly finished. Even Andrew King, who usually eats like a budgie
on a hunger strike, had seconds! (Pic CS03 above) It’s clear to see where
Andre got his talent from, as Pops Frans van Dyk has the same
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PROJECT - Sandstone Coach Re-Wiring (220V) :
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Fred Sewell is cool!
A bit crusty at times … but generally
cool.
Not many people can rewire a coach in one
afternoon – including tea breaks!
He’s done so many coaches in his time at
the Steamreefers that he confidently approached this old creak box with a
fully laid-on pre-prepared coach wiring kit and had the interior cabin lighting
circuits all tested and running on 220V by the time evening came around. Our
own coaches, sleepers and day-sitters alike, have all gradually been
converted to 220V mains power, from the original 24V DC power. The SAR coaches
used to run with massive lead-acid battery racks under-slung from their
bellies, and self tensioned dynamos driven by belts running from one of the
inner bogie axles. Thus, the trains would switch from generator power while
moving to battery backup when standing still.
The systems had inherent problems.
Firstly the weight of the generators and wet-electrolyte lead-acid batteries
added materially to the weight of the coaches. The batteries, their
terminals and their external cell bridges all needed maintenance. The dynamos
and belts themselves would be maintenance items with the bearings,
commutators and brushes all needing attention. And just like the dynamo in
cars of that era, there would also have to be an electromagnetic regulator
for over current, over voltage and the cut-out contacts. The cut-outs were
fitted so the electric current from the batteries would not be able to turn
the dynamos over like a motor, when the dynamo voltage dropped under that at
the battery terminals with the train at standstill.
The lights themselves were prone to
trouble. The open type coaches, such as dining cars and day sitters, had
their 24V inverters mounted inside their DB enclosures but some vehicles had
local inverters inconveniently hidden behind panels. The older discrete-component
transistorized units were prone to failure, and an inverter driven lamp uses
more energy anyway. (Due to the extra losses involved in driving the
inverter’s oscillator and transformer set.) Lastly, a low voltage system inherently
requires higher currents to transmit a decent wattage – so in respect to the
power actually used for lighting and circuits, the inter-coach electrical
connections had to be over-engineered to handle the extra amperage. A faulty
connector would materially reduce the voltage on all the coaches downstream
of the poor joint, due to the series voltage drop across the coupler. And
when you’ve only got 24 volts to play with in the first place – the two or so
volts lost is already a tenth of the capacity.
The new AC powered mains system has the
advantage of being able to use common domestic and industrial fittings and
wiring. It’s also easily compatible with the depot buildings and is ideal
for coupling up to ground power. With the modified coaches of both
Reefsteamers and Shongololo Express, it’s not too unusual to see the train’s lights
burning but the generator van is silent. It also means that in the event of
a generator van failure, standard retail or industrial generators can be used
to power the train. The electrical connections must have thicker insulation
to withstand the voltage – but the current draw relative to the wattage is
much reduced. Thus, a bad connector won’t have such an effect on the coaches
downstream. (Less current through the resistance of a bad joint means a
lower voltage drop.) The elimination of the inverters and in some cases,
transformers, improves both the reliability of the electrical system (less components
to break) and also the efficiency, as you’ve eliminated the inverter quiescent
and oscillator losses, as well as the hysteresis and impedance losses of the
transformers. As our trains are wired for three phase power – a failure on
one line doesn’t black out the entire train.
Anyway – lecture over and onto the
practical stuff.
There are two of the Sandstone-ex-Stilfontien
Mine day-sitter coaches standing in the open area of the eastern Workshop Yard.
Coach No.25163, in the No.2 road, was the coach being rewired today – 2nd
August. (Pic CW01 Below) The sister day-sitter coach, No.25206, is in a bit
of a mess with all the seats unbolted and stacked, and the badly delaminated
floor covering completely removed for re-laying. So Fred got to start his
sparky work on a reasonably intact coach. He had already prepared his inter-coach
plugs and the fly leads during the week, and you can see the coach wiring kit
in Pic CW02. (Below)
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