1932
40HP Crossley horizontal single cylinder engine
saved and restored
The
Villiersdorp branch of the West Cape Tractor & Engine society are busy with
an interesting project, and they're working to a deadline! Just on 13 months
ago we decided to make the recovery and restoration of a 1932 40 HP single
cylinder horizontal Crossley diesel engine a team effort, and we have
advertised that it will be ready and running on 21st June 2008!

Our
first deadline was to strip and remove it from its original place of work,
Standard Roller Mills in Caledon, as the building had been sold and there was a
danger that it would be cut up for scrap. Once the Villiersdorpers get stuck
into something, there's no holding them back! Large teams of helpers turned up
to push and lift and in the space of two Saturdays, there was nothing left in
the engine room!


A
while later a team assembled and with donated steel, we made a rigid steel
framework.

Most
of our members are fruit farmers, so the project was put on hold for the
season. As soon as the last apple was off the trees, we got stuck in and did
the last welds and strengthening on the framework and started cleaning,
painting and repairing the parts. The next weekend, we put the block onto the
frame and then refitted the flywheel to the crank, and put the whole lot
together
Then
we loaded it and took it to its new home, the Villiersdorp Tractor & Engine
museum:

Once
again a large team assembled to move it into position:

Once
in position with a plastic sheet under it, we arranged for the base to be
filled with concrete. This was done early in the week and by the next Saturday
we could start assembling the engine.

The
concrete adds another ton +, to say nothing about rigidity. Then having cleaned
and painted the side shaft and bits at the workshop first, it was sideshaft
assembly on

With
attention to the timing marks. From the cam end:

That's
the basics, wait till you see what it looks like assembled! But Willem is there
painting the flywheel, Josmi was too (taking care not to paint over the
shipping details on one of the spokes!)

In
the background, the new slab which was done at the same time, so we can get in
and out with the forklift. We'll be collecting money for that on the 21st, (we
have a plan to auction off a Fergy)....

Nick
and Eniel feeding pipes through, the right way past various obstacles, until
the sideshaft area looked like this:

Even
then there were some pipes to thread through, cleaning, polishing and flushing
them:

At
the end, we decided to check if we had compression. A bad blow through the
inlet valve, which for some reason we hadn't checked, so that came out again.
It has just struck me that it might have been between the assembly and the
head, so I'll check the seating of the valve in the cage first with a leakage
test, but we took that off:

Looking
towards the rear of the engine, the cover is on properly, it hinges back nicely
against the rests, the shims are in on the big end, and there was a multitude
of work involved with the detailed parts of the sideshaft assembly!
Again
a nice, willing team, not as big as last week, but just right! Mrs Nick again
brought a huge pile of sandwiches and coffee at lunch time to keep us going.
I arrived late at 9am, but we went straight through until 7.30, hardly
stopping. It was amusing to get a call from Graham Bowles from Baynesfield Museum in Natal during the morning, comparing notes.... they were busy at the same
time up there with their Crossley HD9!
There
is still a lot to do, but I think we're on track for the Big Day on the
21st!
Updated
3rd July
2008 (from June 21st activity)
Back
at our Museum the next Saturday, we refitted the machined and lapped inlet
valve assembly, so we could swing the engine and feel for compression. No
problems there!

The
business side of the engine, fully assembled, only pipework to be connected.
The troublesome air start valve control gear is partly obscured by the inlet
valve push rod. The weighted throw-over lever still has to be fitted to the
fuel change-over valve, bottom right of centre.
Nic
had been busy in the week with the artist's brush and a pot of gold paint and
by the end, that made all the difference to the appearance of the engine! Then
various fluids had to be connected, fuel, water in and out (and a tank frame
made and tank installed) exhaust and compresed air. The air bottle, a long
torpedo, still had a bit of air in when we removed it, but this was pressure
tested and certificated.

Nic
has picked out the lettering with gold paint, really finishing the appearance
off smartly! The water inlet plumbing is now fitted and painted. A hydraulic
hose connects the engine to the air receiver.
During
assembly, we re-checked the crankshaft alignment and shimmed and adjusted the
outrigger bearing so that we had less than .001" deflection all round.

Nic
watching the reading on the crankshaft deflection gauge.

Remember
the exhaust pipe I 'felled' from the top of the roof just 13 months ago? Up it
goes again! The water tank is an original air-tight shipping container, said
to have been invented by Richard Trevithick.
We
did not dare leave it to the Great Day before attempting to start! Although we
didn't admit it, we had started it the previous Saturday, then again on the
following Monday which was a Public Holiday and again on the Friday evening
before the official start up. Each time we had found and overcome several
technical problems.
Most
of the problems arose from the fuel injection system. First the main plunger
was seized in its packing. Then all the packings leaked and as a result the
governor (from which we removed one spring which brought the speed down from
its rated 310 to 230 RPM) was unable to maintain the speed correctly.
There are packings on the main fuel pump plunger and one each on the injector
spindle and governor dump valve. Every time we got to a stage where there were
minimal leaks, the governor could hold speed smoothly and accurately. When
anything leaked, the governor hunted, as if saying, 'But I am
giving you enough fuel!'
Another
problem was experienced with the crude/distillate change-over valve which we
thought was stuck, but actually we didn't understand how it works. It has a
weighted throw-over handle which when flicked over towards the engine, opens a
valve allowing the crude (in our case normal fuel, either diesel or
illuminating paraffin) in from the main tank. If it is flicked outwards, it
closes this valve and allows diesel to be drawn in from the small container on
the engine, against a light spring-loaded mitre valve. If there's any
restriction in the main supply then this valve is pulled open by the suction
from the injection pump and it will be exhausted quickly and air will follow!

Ready
to start on the Great Day!
On
the Friday evening, we tried to pump up the compressed air bottle. We had not
overhauled the control valve for the air charging and admission. If we had, we
might have overlooked the leakage between the upper valve and its guide. This
bled air off profusely, making it impossible to charge anything more than 150
PSI (the gauge has a red line at 250 PSI). When trying to start, air was again
being lost down the stem. At least we now understand how it works and can
deal with its repair accordingly.
So,
for the Great Day, we had to resort to belting the engine up to an
International U4 stationary Engine brought along by Denis and this performed
well. It has a clutch, so when the engine fired it could be disengaged
easily and the belt flicked off.
However,
there was a surprise in store! Harvey, whose family owned the building and
mill at which the engine worked, mentioned that his cousin, Uncle Bert
Metcalf, now in his late 70s had first been allowed to start the engine from
the age of 14. He was asked to attend the Start-up, and to show us how he
still remembered to set it in motion!

Uncle
Bert Metcalf looks really happy, feeling his father's engine running again!
Cousin Harvey Metcalf did a lot to secure the engine from being scrapped.
Uncle
Bert was able to tell us stories about the engine, for instance, of how
his father used to count the beats of the engine from his office, and if he
didn't get 12 in any 5 seconds, he knew something was wrong!
About
100 people collected at the Museum on the morning of Saturday 21st June. A few
short speeches were made and the engine was set in motion, settling down to
230 RPM. There was a spontaneous round of applause and many looks of
wonderment on the spectators' faces!

Running
again!
Finally, two
very happy faces on the Main Conspirators! To those many people not mentioned
here, many thanks, too, for your help. As I mentioned in my (short) speech,
the restoration of an engine of this size is best tackled by a group. Apart
from any work carried out in the week, all the work was accomplished in the
space of just nine Saturdays. Best of all, we all enjoyed it so much, making
fun of each other unmercifully! We also got to know one another much better,
which is what a hobby is all about!
Two
more happy faces, Andy Selfe and Eniel Viljoen
Now
to persuade the Team to tackle the Clayton & Shuttleworth Trusty next!
Andy
Selfe